N3213C

Substantial
None

BEECH E35S/N: D-3877

Accident Details

Date
Thursday, November 20, 2008
NTSB Number
CEN09CA080
Location
Bloomington, IN
Event ID
20081203X10613
Coordinates
39.146110, -86.616668
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A partial loss of engine power due to a failure of the number one cylinder exhaust valve, and the associated secondary damage to the intake valve and piston.

Aircraft Information

Registration
N3213C
Make
BEECH
Serial Number
D-3877
Engine Type
Reciprocating
Year Built
1954
Model / ICAO
E35BE35
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SIX FOUR ALPHA LLC
Address
3511 SILVERSIDE RD STE 105
Status
Deregistered
City
WILMINGTON
State / Zip Code
DE 19810-4902
Country
United States

Analysis

The pilot reported that the engine began to run rough during cruise flight at 6,000 feet mean sea level (msl). He noted that the takeoff and climb were uneventful, and the personal instrument flight rules (IFR) flight had proceeded normally to that point. He advised air traffic control of the situation and elected to divert to an intermediate airport located approximately 10 miles west of his present position. The pilot increased the mixture, switched fuel tanks, and applied carburetor heat in an attempt to address the rough running engine; however, those efforts were not successful. The #1 cylinder temperature had dropped and the engine oil pressure subsequently went to zero. He notified the controller that he would be unable to make it to the runway and set up for a forced landing in a pasture about 3.5 miles east of the airport. The terrain consisted of rolling hills. After touch down, he was unable to stop the airplane before it impacted a fence and trees. The airplane sustained substantial damage to the leading edges of both wings. A post accident inspection revealed that the #1 cylinder exhaust valve had failed at the base of the valve stem. The intake valve and piston sustained mechanical damage as a result. The secondary mechanical damage precluded a metallurgical examination of the fracture surface of the exhaust valve stem. The Continental E225-8 engine that powered the airplane had accumulated about 1,130 hours since overhaul. The airplane had accumulated about 26 hours flight time since the most recent annual inspection, which was completed approximately one month prior to the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN09CA080