N7176W

Substantial
Minor

ROBINSON HELICOPTER R22 BETAS/N: 2735

Accident Details

Date
Wednesday, July 29, 2009
NTSB Number
WPR09CA375
Location
Troutdale, OR
Event ID
20090729X43708
Coordinates
45.520244, -122.350593
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The flight instructor's failure to maintain adequate main rotor RPM.

Aircraft Information

Registration
N7176W
Make
ROBINSON HELICOPTER
Serial Number
2735
Engine Type
Reciprocating
Year Built
1997
Model / ICAO
R22 BETAR22
Aircraft Type
Rotorcraft
No. of Engines
1

Registered Owner (Historical)

Name
HILLSBORO AVIATION INC
Address
3565 NE CORNELL RD
Status
Deregistered
City
HILLSBORO
State / Zip Code
OR 97124-6374
Country
United States

Analysis

After practicing a series of autorotations, the flight instructor and his student attempted to complete a 180-degree autorotation. The student began a stabilized autorotation from the downwind leg of the traffic pattern. According to the flight instructor, during the turn the student allowed the nose of the helicopter to drop; he was instructed to correct this attitude by applying aft cyclic. When the student completed the turn at an altitude of 200 to 250 ft agl and at a speed of 80 to 85 knots, the flight instructor believed that the outcome of the maneuver was in doubt. The flight instructor then took control of the helicopter and began to initiate a recovery by raising the nose and attempting to increase the throttle and collective to arrest the descent rate. According to the flight instructor, the RPM decayed and the low rotor rpm horn came on at 150 to 100 ft agl. The helicopter landed hard and subsequently slid off the north side of the taxiway. The forward section of the left skid contacted the soft dirt, which resulted in the helicopter turning to the left and nosing over. Examination of the aircraft by a Federal Aviation Administration inspector revealed substantial damage to the helicopter consisted of the separation of the tail boom assembly, damage to the firewall, the left forward frame, and left skid support structure. The flight instructor reported no mechanical anomalies with the helicopter or flight control systems.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR09CA375