N6233V

Substantial
Serious

MUFFETT QUICKSLVR SPRNT IIS/N: 1992 SPRINT 395

Accident Details

Date
Thursday, March 4, 2010
NTSB Number
WPR10LA150
Location
Buena, WA
Event ID
20100304X43317
Coordinates
46.443054, -120.340835
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A loss of engine power due to fuel exhaustion as a result of the student pilot’s inadequate fuel planning.

Aircraft Information

Registration
N6233V
Make
MUFFETT
Serial Number
1992 SPRINT 395
Engine Type
Reciprocating
Year Built
1993
Model / ICAO
QUICKSLVR SPRNT IISBM3
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
DART JOSEPH O
Address
PO BOX 303
Status
Deregistered
City
EATONVILLE
State / Zip Code
WA 98328-0303
Country
United States

Analysis

On March 3, 2010, at 1653 Pacific standard time, an experimental Muffett Quicksilver Sprint II, N6233V, sustained substantial damage following a loss of engine power and subsequent forced landing shortly after takeoff from the Buena Airport, Buena, Washington. The airplane, which is owned by the student pilot, was operated as a visual flight rules (VFR) personal flight under the provisions of 14 Code of Federal Regulations (CFR) Part 91, when the accident occurred. The student pilot, the sole occupant of the airplane, sustained serious injuries. Visual meteorological conditions prevailed for the local flight that originated from Buena.

During a telephone conversation with the National Transportation Safety Board (NTSB) Investigator-in-charge (IIC) on March 5, 2010, the student pilot stated he was practicing touch-and-go landings at the private airstrip. After approximately 10 landings, the pilot taxied the airplane back to the parking area where he met with a friend (the former owner of the airplane) and discussed the flight. After a short conversation the pilot taxied to the departure end of the runway and departed to the east. He reported that shortly after takeoff the engine lost power and he attempted to land in a nearby field. The airplane subsequently impacted terrain, which resulted in substantial damage to the fuselage and wing assembly. The pilot attributed the loss of engine power to a lack of fuel, stating that the airplane simply ran out of gas.

An acquaintance of the pilot (and former owner of the airplane) reported that he heard the airplane takeoff. He reported that during the initial climb, approximately 200 feet above ground level (agl), he heard the airplane's engine "quit" and looked up to see the airplane in a “stalling descent.” He reported that approximately 80 feet agl the airplane “broke over” and collided with terrain in a nose-low attitude. The acquaintance went to the accident site to assist the pilot. He reported that while at the site, he observed no fuel in the fuel tank, lines or filter. He further reported that the student pilot had run out of fuel on two previous occasions.

The pilot did not submit a Pilot/Operator Report, Form 6120.1. Multiple attempts to contact the pilot following the March 5 telephone conversation were not successful.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR10LA150