Summary
On February 27, 2010, a Grumman American AA-5 (N5418L) was involved in an incident near Maple Lake, MN. All 2 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's failure to maintain a proper glide path during a simulated forced landing and the flight instructor's delayed remedial action to execute a go-around.
The pilot attempted a simulated forced landing at the airport by entering the traffic pattern for a landing on runway 28 (2,796 feet by 60 feet, asphalt) during an instructional flight. During final approach, the pilot realized the airplane was not going to reach the runway and attempted a go-around. The airplane impacted the ground about 700 feet short of the runway resulting in substantial damage to the airplane structure underlying the nose landing gear. The pilot and flight instructor were uninjured. The airplane had not been registered since its purchase by the current aircraft owner. There was no report made of an incident/accident to the National Transportation Safety Board (NTSB) or Federal Aviation Administration until March 3, 2010, at which time the pilot contacted the NTSB.
This incident is documented in NTSB report CEN10CA154. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N5418L.
Accident Details
Probable Cause and Findings
The pilot's failure to maintain a proper glide path during a simulated forced landing and the flight instructor's delayed remedial action to execute a go-around.
Aircraft Information
Registered Owner (Historical)
Analysis
The pilot attempted a simulated forced landing at the airport by entering the traffic pattern for a landing on runway 28 (2,796 feet by 60 feet, asphalt) during an instructional flight. During final approach, the pilot realized the airplane was not going to reach the runway and attempted a go-around. The airplane impacted the ground about 700 feet short of the runway resulting in substantial damage to the airplane structure underlying the nose landing gear. The pilot and flight instructor were uninjured. The airplane had not been registered since its purchase by the current aircraft owner. There was no report made of an incident/accident to the National Transportation Safety Board (NTSB) or Federal Aviation Administration until March 3, 2010, at which time the pilot contacted the NTSB.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN10CA154