N1257E

Substantial
None

DEARMOND CLINT RV-6AS/N: 60369

Accident Details

Date
Sunday, May 16, 2010
NTSB Number
CEN10LA253
Location
Sheboygan, WI
Event ID
20100517X21204
Coordinates
43.769721, -87.851669
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The loss of engine power due to a fuse failure in the ignition system.

Aircraft Information

Registration
Make
DEARMOND CLINT
Serial Number
60369
Engine Type
Reciprocating
Model / ICAO
RV-6A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
RV-6A

Registered Owner (Current)

Name
WUNSCH DONALD L
Address
21419 POPLAR GROVE RD
City
REEDSVILLE
State / Zip Code
WI 54230-9229
Country
United States

Analysis

On May 16, 2010, at 1115 central daylight time, a Dearmond RV-6A single-engine experimental airplane, N1257E, sustained substantial damage during a forced landing following a loss of engine power near Sheboygan, Wisconsin. The private pilot, who was the sole occupant and registered owner, was not injured. Visual meteorological conditions prevailed and no flight plan was filed for the Title 14 Code of Federal Regulations Part 91 personal flight. The local flight departed Manitowoc, Wisconsin, at 1020.

According to the pilot, while cruising at 2,900 feet above ground level (agl), he advanced the throttle and heard a "pop" from the engine. The engine lost total power and the propeller stopped. The pilot's engine restart was unsuccessful, and he attempted to land at the nearest airport. The airplane landed short of the airport runway in a muddy field. During the landing, the nose landing gear collapsed and the airplane nosed over.

Examination of the airplane by the pilot and Federal Aviation Administration inspectors revealed the vertical stabilizer and rudder were bent.

Detailed examination of the airframe and engine revealed that a 7.5 amp ignition fuse, located in the empennage of the airplane, had failed during the flight, which resulted in the loss of ignition and the inability to restart the engine. The pilot stated that he was unaware of this fuse in the ignition system. The airplane's most recent conditional inspection was completed on June 28, 2009, and the airplane had accumulated 330.8 total hours at the time of the accident.

The pilot's medical certificate was expired and his flight review was not current.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN10LA253