Summary
On May 17, 2010, a Nelson Steven Paul WAG-AEROSPORTSMAN2+2 (N124SN) was involved in an incident near Milica, MN. All 2 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: A loss of engine power due to fuel starvation as a result of the pilot's inadequate in-flight fuel management.
According to the pilot, he and his passenger had flown for approximately 1.5 hours prior to returning to his airport for landing. Prior to landing, the pilot became distracted by other aircraft within the vicinity of the airport and "[the pilot] forgot to switch to 'both' [tanks] on the fuel selector." During the landing, the airplane bounced and the pilot executed a go-around in order to perform "a better landing." While executing a go-around, the engine lost power. The pilot attempted to land on the remaining runway; however, the airplane touched down in a field and the left main landing gear collapsed. The pilot reported that he forgot to switch fuel tanks during the flight and that was the reason the engine lost power.
This incident is documented in NTSB report CEN10CA254. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N124SN.
Accident Details
Probable Cause and Findings
A loss of engine power due to fuel starvation as a result of the pilot's inadequate in-flight fuel management.
Aircraft Information
Registered Owner (Current)
Analysis
According to the pilot, he and his passenger had flown for approximately 1.5 hours prior to returning to his airport for landing. Prior to landing, the pilot became distracted by other aircraft within the vicinity of the airport and "[the pilot] forgot to switch to 'both' [tanks] on the fuel selector." During the landing, the airplane bounced and the pilot executed a go-around in order to perform "a better landing." While executing a go-around, the engine lost power. The pilot attempted to land on the remaining runway; however, the airplane touched down in a field and the left main landing gear collapsed. The pilot reported that he forgot to switch fuel tanks during the flight and that was the reason the engine lost power. Examination of the airplane revealed the left main wing spar was bent.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN10CA254