N128AF

Substantial
None

NORTH AMERICAN T-28AS/N: 491619A

Accident Details

Date
Thursday, May 27, 2010
NTSB Number
CEN10LA272
Location
Oklahoma City, OK
Event ID
20100528X02042
Coordinates
35.601943, -97.706108
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The failure of the master rod bearing, which resulted in a loss of engine power.

Aircraft Information

Registration
N128AF
Make
NORTH AMERICAN
Serial Number
491619A
Engine Type
Reciprocating
Year Built
1949
Model / ICAO
T-28AT28
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WILLIAMS THOMAS C
Address
11740 HACKNEY LN
Status
Deregistered
City
YUKON
State / Zip Code
OK 73099-8129
Country
United States

Analysis

On May 27, 2010, about 2010 central daylight time, a North American T-28A airplane, N128AF, was substantially damaged following a loss of engine power and subsequent forced landing at Sundance Airpark (HSD), Oklahoma City, Oklahoma. The commercial pilot and the certified flight instructor were not injured. The local, personal flight was being conducted under the provisions of 14 Code of Federal Regulations Part 91 without a flight plan. Visual meteorological conditions prevailed at the time of the accident.

The pilots stated they were flying in the traffic pattern when the engine started losing power. They were unable to make the runway and landed short of the prepared surface. Postaccident examination of the airplane revealed the main landing gear had punctured both wings, damaging the spars, and two engine mounts had pulled loose from the firewall. Fuel was found in both wings and the fuel selector was in the BOTH position. Metal material was found in the outer casing of the oil filter. According to one of the airplane’s owners, the engine was later disassembled for salvage and the master rod bearing was found failed and several of the cylinders had seized.

According to maintenance records, the engine’s last major overhaul occurred on August 15, 1989. The last annual inspection occurred on December 5, 2009, at 77.7 hours time since major overhaul. According to the operator of the airplane, it had accumulated 99.9 hours time since major overhaul at the time of the accident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN10LA272