N196DN

MINR
None

BOEING 767

Accident Details

Date
Wednesday, June 16, 2010
NTSB Number
ENG10IA038
Location
Athens, Greece
Event ID
20100617X02311
Aircraft Damage
MINR
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A short circuit involving the light in position L3 on the squib test panel. The specific cause of the short circuit could not be determined.

Aircraft Information

Registration
Make
BOEING
Engine Type
Turbo-fan
Year Built
1997
Model / ICAO
767B762
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
330
FAA Model
767-332

Registered Owner (Current)

Name
DELTA AIR LINES INC
Address
1775 M H JACKSON SERVICE RD
DEPT 595 AIRCRAFT REGISTRATIONS
City
ATLANTA
State / Zip Code
GA 30354-3743
Country
United States

Analysis

On June 16, 2010, at 1330 UTC, Delta Air Lines flight 139, a B767-332ER, registered as N196DN, experienced a cockpit fire during preflight preparations at Eleftherios Venizelos International Airport (LGAV). The fire occurred prior to passenger boarding, and there were no injuries to the 3 flight crew and an unknown number of cleaning crew personnel on board the aircraft. During the preflight process, ground maintenance personnel performed a "push to test" on the right sidewall accessory panel (P61). After an undetermined period of time, while the first officer continued with his preflight procedures, he smelled smoke and then observed a flame coming out from the right sidewall accessory panel. He extinguished the fire by using a halon fire extinguisher. The investigation was delgated to the NTSB by the Hellenic Air Accident Investigation and Aviation Safety Board.

The panels involved with the fire (the squib test panel and the miscellaneous test panel) were removed and sent to Boeing's Engineering Quality Analysis (EQA) laboratory in Seattle, WA. On September 16, 2010, the panels were examined under the direction of the NTSB.

The existing condition of the panels submitted for examination was documented, tests were conducted where possible, and chemical analyses were conducted on some samples. The damage on the squib test panel was most severe around the light in position L3.

During tests of the L3 light, the resistance between terminals 2 and 3 varied from 0.6 ohms to 4.6 ohms. Based on the damage to L3, it could not be determined if a short initiated as a result of physical damage, a conductive path of contaminants, a workmanship error that may have been created when L3 was removed and replaced, or a manufacturing defect with the lamp itself.

While only 14 ohms were measured between terminals 1 and 2 of L3, it is believed that this short occurred after the press to test was performed per the pre-flight process and a result of the heat generated from the short between terminals 2 and 3. If this value actually existed during the pre-flight, the current would have been significant enough to discharge the fire bottles. The fire bottles were not discharged during the incident.

Switch S5 on the miscellaneous test panel showed evidence of heat damage on the bottom of the switch. Switch S5 on the miscellaneous test panel is almost directly above light L3 on the squib test panel.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ENG10IA038