N4596U

Substantial
Minor

CESSNA U206GS/N: U20604990

Accident Details

Date
Wednesday, June 30, 2010
NTSB Number
ANC10LA056
Location
Iliamna, AK
Event ID
20100630X12540
Coordinates
59.648334, -155.419998
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
5
Total Aboard
6

Probable Cause and Findings

The total loss of engine power during cruise flight due to a fractured crankshaft.

Aircraft Information

Registration
Make
CESSNA
Serial Number
U20604990
Engine Type
Turbo-shaft
Year Built
1979
Model / ICAO
U206GC206
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
U206G

Registered Owner (Current)

Name
RUSTAIR INC
Address
PO BOX 190867
City
ANCHORAGE
State / Zip Code
AK 99519-0867
Country
United States

Analysis

On June 29, 2010, about 1745 Alaska daylight time, a float-equipped Cessna U206G airplane, N4596U, sustained substantial damage to the wings, rudder and fuselage during an emergency off-airport landing, about 16 miles west-southwest of Iliamna, Alaska. The airplane was operated by Rust's Flying Service, Anchorage, Alaska, as a visual flight rules (VFR) revenue sightseeing flight under 14 Code of Federal Regulations, Part 135, when the accident occurred. The commercial pilot and four passengers were not injured; the remaining passenger received minor injuries. The flight was returning to the operator's base at the Lake Hood Seaplane Base, Anchorage. Company flight following procedures were in effect.

During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), a representative for the operator said the pilot reported a complete loss of engine power that precipitated an emergency descent, and off-airport landing. The pilot reportedly told him he saw a rise in the exhaust gas temperature (EGT) prior to the loss of power. The float-equipped airplane landed on tundra-covered ground and nosed over. The pilot reported adding 42 gallons of aviation fuel prior to the return flight to Anchorage.

In a written statement to the FAA dated July 1, the pilot wrote that about 40 minutes into the flight he saw the EGT rise above the normal cruise temperature. He enriched the mixture from 15 gallons per hour (GPH) to 18 GPH, to cool the engine. Shortly thereafter the engine quit completely. After several failed attempts to restart the engine, he focused on landing the airplane.

On August 18, the airplane was examined by the NTSB IIC at an airplane maintenance facility in Wasilla, Alaska. During an attempt to rotate the propeller, it was discovered that the propeller would not rotate, and the rear accessory portion of the engine did not appear to be connected through the crankshaft to the propeller.

On November 9, the airplane's engine was disassembled at an airplane maintenance facility in Palmer, Alaska. In attendance with the IIC were representatives from the FAA, and the engine manufacturer. During the disassembly it was discovered that the engine's crankshaft had fractured, and separated at the number 2 journal.

The crankshaft was shipped to the NTSB material laboratory, Washington, D.C., for examination. The laboratory engineer found "ladder cracking," indicative of oil starvation, associated with the journal fracture. The NTSB material laboratory report is contained in the public docket for this report.

Engine History

Prior to October 21, 2008 the accident airplane's engine, serial number 286450-R was overhauled by Aero Recip, Anchorage, Alaska. The overhauled engine was sold to Mulchatna Air, Dillingham, Alaska, and installed in one of their airplanes. During the first flight, the engine lost oil pressure, the pilot landed, and the engine oil filter was checked for metal particles. Finding metal in the filter, the owner requested the engine be replaced by Aero Recip, which it was. During a telephone conversation with the NTSB IIC, the owner of Mulchatna Air said a couple days after returning the engine, he received a telephone call from Aero Recip, stating they could not find anything wrong with the engine, and they were returning it to service.

According to the engine's log book, on June 24, 2009, the engine was removed from the airplane due to possible metal contamination. The engine was partially disassembled by Aero Recip, and inspected. No contamination was found, so the engine was reassembled, and test run three times. After each run the oil filter was examined, with no notable contaminates or ferrous metal found. Aero Recip returned the engine to service.

On July 7, 2009 the engine was installed in the accident airplane. At the time of the accident, the engine had 441 hours of operation since the October 21, 2008 major overhaul.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC10LA056