N132AT

Substantial
Minor

DOUGLAS A4LS/N: 12374

Accident Details

Date
Thursday, July 8, 2010
NTSB Number
WPR10LA339
Location
Fallon, NV
Event ID
20100708X82843
Coordinates
39.455001, -118.731941
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A loss of engine power during takeoff due to the failure of the engine's stator and turbine. Contributing to the accident was inadequate maintenance.

Aircraft Information

Registration
N132AT
Make
DOUGLAS
Serial Number
12374
Engine Type
Reciprocating
Year Built
1960
Model / ICAO
A4LDC4
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
4

Registered Owner (Historical)

Name
A-4L LLC
Address
8191 E KAISER BLVD
Status
Deregistered
City
ANAHEIM
State / Zip Code
CA 92808-2214
Country
United States

Analysis

On July 8, 2010, about 1340 Pacific daylight time, a Douglas A4L, N132AT, collided with terrain after the pilot ejected following a loss of engine power on takeoff from Fallon Naval Air Station, Fallon, Nevada. Airborne Tactical Advantage Company (ATAC) was operating the airplane under the provisions of 14 Code of Federal Regulations (CFR) Part 91 on a local public-use flight. The airline transport pilot sustained minor injuries. The airplane sustained substantial damage by impact forces and post crash fire. Visual meteorological conditions prevailed, and no flight plan had been filed.

The operator reported that the takeoff and gear and flap retraction were normal. The pilot started a right turn for departure from the airport traffic area during the initial climb when the engine lost power. He reversed his turn, and attempted to land on the runway in the opposite direction of the takeoff. The airplane was too low and slow, so he steered the airplane in the direction of an empty field and successfully ejected. The airplane exploded on impact.

The operator reported that their examination of the engine determined that the protective coating on the turbine blades and stators had degraded. This degradation led to the eventual failure of the stator vanes and then the turbine blades. They could not establish the exact reason for the degradation of the protective coating.

The operator listed several contributing factors. They were unaware of a requirement to down trim the engines to a maximum of 102 percent until an associated technical change had been complied with. The airplane had a modified electrical start system that resulted in starts that approached the flight manual time and temperature maximum limits. During the post accident exam, they discovered a broken fuel tube due to fatigue in the combustion chamber at the 11 o'clock position.

The operator believes that none of the contributing conditions caused the engine problem. However, they stated that the combination of the three led to the degradation of the protective coatings on the stators and blades in the turbine section, and ultimately the failure of the turbine blades.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR10LA339