N48417

Substantial
None

GRUMMAN G164S/N: 26B

Accident Details

Date
Friday, October 1, 2010
NTSB Number
ERA11LA011
Location
Edison, GA
Event ID
20101007X11802
Coordinates
31.559999, -84.750000
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Leakage of hydraulic fluid from the internal fuselage line fitting, resulting in a subsequent loss of the right brake’s effectiveness.

Aircraft Information

Registration
N48417
Make
GRUMMAN
Serial Number
26B
Engine Type
Turbo-shaft
Year Built
1976
Model / ICAO
G164G64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HUMPHREY B FLYING LLC
Address
7303 MAYNARD WHEELER LN
Status
Deregistered
City
TERRE HAUTE
State / Zip Code
IN 47803-9561
Country
United States

Analysis

HISTORY OF FLIGHT

On October 1, 2010, about 1630 eastern daylight time, a Grumman G-164B, N48417, was substantially damaged following a runway excursion during landing at a private airfield in Edison, Georgia. The certificated commercial pilot was not injured. Visual meteorological conditions prevailed, and no flight plan was filed for the local aerial application flight, which was conducted under the provisions of Title 14 Code of Federal Regulations Part 137.

The pilot departed the private, turf runway on a routine application flight. He stated that during the flight, as he applied rudder pedal during turns, he felt that the right pedal was "soft," but stated that the left rudder pedal felt normal. He returned to the airport at the conclusion of the flight and just after touchdown, applied pressure to both brake pedals to stop the airplane. The pilot stated that the right pedal depressed to the floor and was ineffective, but the left pedal and left brake operated normally. The pilot applied reverse engine thrust, but the airplane continued left and departed the runway, where it came to rest upright.

The airplane was examined at the accident site by a Federal Aviation Administration (FAA) inspector. The right main landing gear separated from the airplane, and both left and right upper and lower wings sustained substantial damage.

PERSONNEL INFORMATION

The pilot held a commercial pilot certificate with ratings for airplane single and multi engine land, instrument airplane, and rotorcraft helicopter. He reported 7,700 total hours of flight experience, approximately 4,000 hours of which were in the accident airplane make and model. His most recent flight review was completed in June, 2009. His most recent FAA second-class medical certificate was issued in March 2010 with no limitations.

AIRCRAFT INFORMATION

According to FAA records, the airplane was manufactured in 1976 and was powered by a Walter M601E-11 turbine engine, which was equipped with a three-bladed, Hamilton Standard propeller. The pilot stated that approximately one year prior to the accident, the airplane experienced a right brake failure during landing, but he was able to maintain control and the airplane sustained no damage. Subsequent inspection of the right brake master cylinder revealed a worn o-ring, which was replaced. The airplane's most recent annual inspection was completed on April 9, 2010, at which time the airplane had accumulated a total of 12,500 hours. The airplane's maintenance logs revealed that both left and right landing gear brake pads and all wheel bearings were replaced as part of the inspection.

METEOROLOGICAL INFORMATION

The 1639 weather observation at BIJ, located approximately 13 nautical miles southwest of the accident location, included winds from 320 degrees at 3 knots, 10 statute miles visibility, a scattered cloud layer at 7,500 feet, temperature 28 degrees C, dew point 12 degrees C, and an altimeter setting of 29.79 inches of mercury.

ADDITIONAL INFORMATION

The airplane was recovered from the accident scene, and the right brake system was examined in detail by an FAA inspector. The inspector found evidence of brake fluid leakage at the internal fuselage hydraulic line fitting, but no evidence of leakage was observed at any other point in the system. The right brake line was separated during the accident sequence, and no fluid remained in the upper portion of the system or in the right brake caliper. As such, no reliable measure of the brake fluid quantity could be made as the right brake system had been compromised during the accident. A test line was fabricated, and the system was pressure-tested. Application of pressure at the brake master cylinder produced movement of the caliper, with a corresponding retraction of the caliper when pressure was removed.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA11LA011