N525BD

Substantial
Serious

MISCHKE BD-5BS/N: 2

Accident Details

Date
Thursday, October 14, 2010
NTSB Number
WPR11LA015
Location
Burlington, WA
Event ID
20101015X85729
Coordinates
48.470832, -122.420829
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The failure of the sprag clutch during takeoff, resulting in a loss of engine thrust.

Aircraft Information

Registration
N525BD
Make
MISCHKE
Serial Number
2
Engine Type
Reciprocating
Year Built
2009
Model / ICAO
BD-5BSA02
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MISCHKE DAVID E
Address
7504 FREDRICKSON RD
Status
Deregistered
City
SEDRO WOOLLEY
State / Zip Code
WA 98284-7877
Country
United States

Analysis

On October 14, 2010, at 1140 Pacific daylight time, an experimental Mischke BD-5D, N525BD, impacted the approach end of runway 22 at Skagit Regional Airport, Burlington, Washington. The commercial pilot was operating the airplane under the provisions of 14 Code of Federal Regulations Part 91. The pilot sustained serious injuries; the airplane was substantially damaged. Visual meteorological conditions prevailed and no flight plan was filed for the local area flight.

The pilot submitted a written statement following the accident. After departing runway 10, the airplane rotated at 90 miles per hour (mph), he retracted the landing gear, and accelerated the airplane to 140 mph while climbing to 50 to 75 feet above ground level. The engine revolutions per minute (rpm) increased, then decreased from 9,000 to about 7,000, and he felt a loss of thrust in the airplane. He retarded the throttle and attempted an emergency landing on runway 22. The airplane landed hard short of the runway, with the landing gear retracted.

The pilot reported that the airplane was powered by a Yamaha Nytro snowmobile engine rated at 130 horsepower at 10,000 rpm. The engine ran at 8,000 rpm with the propeller at 4,000 rpm. Examination of the drive system revealed that the sprag clutch that connected the drive system had failed and the engine lost thrust.

A Dynon Avionics EFIS-D10A unit was recovered from the airplane and sent to the Safety Board Recorder Laboratory. Information regarding the flight track, ground, and altitude were obtained from the unit. Because the unit did not have a recent software upgrade, no additional information was recorded.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR11LA015