Summary
On January 25, 2011, a Culver Glenn KITFOX III (N947RG) was involved in an incident near Terlingua, TX. All 1 person aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's loss of directional control on takeoff.
The commercial pilot was practicing touch and go landings on a dirt strip in his single-engine experimental light sport aircraft when he decided to make a full stop landing and taxi back for another take off. While on the take off roll at a high rate of speed, and before the tail was raised, the nose of the airplane veered to the left and the pilot used the right rudder pedal to maintain directional control but accidentally hit the toe brake. As a result, the airplane turned about 110 degrees to the right and the airplane collided with the ground and scrub brush with both wing tips before it came up on its nose. The wooden propeller was shattered and a portion of the airframe and both wings were substantially damaged. The pilot reported there were no pre-mishap mechanical deficiencies.
This incident is documented in NTSB report CEN11CA165. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N947RG.
Accident Details
Probable Cause and Findings
The pilot's loss of directional control on takeoff.
Aircraft Information
Analysis
The commercial pilot was practicing touch and go landings on a dirt strip in his single-engine experimental light sport aircraft when he decided to make a full stop landing and taxi back for another take off. While on the take off roll at a high rate of speed, and before the tail was raised, the nose of the airplane veered to the left and the pilot used the right rudder pedal to maintain directional control but accidentally hit the toe brake. As a result, the airplane turned about 110 degrees to the right and the airplane collided with the ground and scrub brush with both wing tips before it came up on its nose. The wooden propeller was shattered and a portion of the airframe and both wings were substantially damaged. The pilot reported there were no pre-mishap mechanical deficiencies.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN11CA165