N6169Z

Substantial
Minor

CESSNA TU206GS/N: U20606172

Accident Details

Date
Saturday, March 19, 2011
NTSB Number
WPR11LA168
Location
Puyallup, WA
Event ID
20110319X95407
Coordinates
47.103889, -122.286941
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilots’ activation of the fuel boost pump while preparing to land, which was contrary to checklist procedures and resulted in a loss of engine power.

Aircraft Information

Registration
N6169Z
Make
CESSNA
Serial Number
U20606172
Engine Type
Reciprocating
Year Built
1981
Model / ICAO
TU206GC206
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WINGS EXPORT LLC
Address
6490 SE 138TH AVE
Status
Deregistered
City
MORRISTON
State / Zip Code
FL 32668-7265
Country
United States

Analysis

On March 19, 2011, about 1115 Pacific daylight time, a Cessna TU 206G, N6169Z, sustained substantial damage to the forward portion of the fuselage and empennage during a forced landing following a loss of engine power while in the airport traffic pattern at the Pierce County Airport - Thun Field (PLU), Puyallup, Washington. The certified flight instructor and commercial pilot receiving instruction sustained minor injuries. The airplane was registered to the Civil Air Patrol and operated as a local instructional flight under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed and a company visual flight rules flight plan had been activated for the local flight that departed from Puyallup.

A representative from the operator reported that the pilots performed the pre-landing checklist, and switched the fuel selector to the right tank position and activated the auxiliary fuel boost pump while on the left midfield downwind for landing on runway 34. Shortly thereafter, while turning from base leg to final, at 900 feet mean sea level (msl), the airplane began to sink and full engine throttle was applied. The engine subsequently did not power up, and the airplane collided with up-sloping terrain approximately 400 feet short of the approach end of the runway. The nose landing gear collapsed, and the airplane subsequently nosed over.

The airplane was equipped with a Continental TSIO-520-CCM engine. The engine is turbocharged, fuel injected and equipped with a constant speed propeller. The airplane’s fuel system incorporates a 2-stage electric auxiliary fuel boost pump. The fuel pump is placarded “emergency” and “start” and is utilized for engine starts and engine related emergencies.

The manufacturer’s approved checklist for the airplane denotes, in part, the following:

DESCENT

1. Power – AS DESIRED

2. Auxiliary Fuel Pump Switch - OFF

BEFORE LANDING

1. Fuel Selector valve – FULLER TANK

2. Auxiliary Fuel Pump Switch - OFF

A representative from the engine manufacturer reported that operating the auxiliary fuel boost pump at a low engine power setting would “flood” the engine and result in a loss of engine power.

Postaccident examination of the airframe and engine revealed no preaccident mechanical malfunctions or failures that would have precluded engine operations. An engine examination report is contained in the public docket for this case file.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR11LA168