N80WW

Substantial
None

WILEY C W RV-6AS/N: 22709

Accident Details

Date
Monday, June 13, 2011
NTSB Number
CEN11LA385
Location
Colgate, OK
Event ID
20110614X95920
Coordinates
34.530441, -96.210685
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The loss of engine power for undetermined reasons.

Aircraft Information

Registration
N80WW
Make
WILEY C W
Serial Number
22709
Engine Type
Reciprocating
Year Built
1997
Model / ICAO
RV-6ARV6
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WILEY C W DR
Address
477 COUNTY ROAD 4530
Status
Deregistered
City
MOUNT PLEASANT
State / Zip Code
TX 75455-8504
Country
United States

Analysis

On June 13, 2011 about 0900 central daylight time, a Vans RV-6A, kit-built airplane, N80WW conducted a forced landing, after experienced a loss of engine power while in cruise flight near Colgate, Oklahoma. The private pilot, sole occupant, received only minor injuries. The airplane was substantially damaged during the accident. The airplane was registered to and operated by a private individual under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed for the flight, which operated without a flight plan. The flight originated about 0800, from the Mount Pleasant Regional Airport (OSA), Mount Pleasant, Texas, en route to Harper, Kansas.

The pilot reported he departed on the cross-country flight with the airplane’s fuel tanks full; the initial departure and first part of the cruise flight was uneventful. About 40 minutes into the flight, he noticed that the engine’s exhaust gas temperature (EGT) climbed from 1380 F to 1400 F. The pilot subsequently enriched the mixture slightly and the temperature dropped back to 1380 F. The pilot then stated that everything appeared fine; however, approximately 2 minutes later, the higher EGT indication reappeared. The pilot then again enriched the mixture slightly and the EGT reading dropped back to normal. The pilot added that the same circumstances repeated itself a couple more times. Finally, after enriching the mixture all he could, the pilot stated “the engine quit as though someone closed the mixture in a routine shutdown, without any sputtering or coughing”. Unable to restart the engine, he selected a field to conduct a force landing in. During the forced landing, the airplane’s landing gear collapsed and the airplane came to rest in an upright position.

The airplane was recovered to the owner’s hangar for examination.

On July 28, 2011 an investigator from the NTSB and the airplane’s owner examined the airplane. The airplane’s wings and fuselage had sustained heavy damage during the forced landing; the nose landing gear had folded back into the firewall and cabin area. The engine’s carburetor located at the bottom of the engine had sustained impact damage and was broken from away from engine’s sump/intake. Additionally, the carburetor itself was broken by the impact and remained attached to the airplane by the alternate air cable. Both mixture and throttle control attachments were pulled from the carburetor. The carburetor finger and airplane’s fuel line gascolator screens were absent any contaminates or debris. Both fuel tanks were breeched during the accident; air was blown into the fuel line and through the fuel selector towards the fuel tanks. The fuel lines and fuel tank pickup points appeared clear without abnormalities. The engine driven fuel pump was partially disassembled and no abnormalities noted. A reason for the loss of power was not found.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN11LA385