N8319N

Substantial
None

PIPER PA-32R-301S/N: 32R-8113029

Accident Details

Date
Saturday, July 2, 2011
NTSB Number
ERA11LA386
Location
Louisville, KY
Event ID
20110707X01459
Coordinates
38.227779, -85.663612
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
4
Total Aboard
4

Probable Cause and Findings

The pilot's improper flare and inadequate recovery from a bounced landing, which resulted in a landing gear collapse.

Aircraft Information

Registration
Make
PIPER
Serial Number
32R-8113029
Engine Type
Reciprocating
Year Built
1980
Model / ICAO
PA-32R-301P32R
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
7
FAA Model
PA-32R-301

Registered Owner (Current)

Name
MAX Q AVIATION LLC
Address
55 N 4TH ST UNIT 202
City
COCOA BEACH
State / Zip Code
FL 32931
Country
United States

Analysis

On July 2, 2011, about 1430 eastern daylight time, a Piper PA-32R-301, N8319N, operated by a private pilot, was substantially damaged while landing at Bowman Field Airport (LOU), Louisville, Kentucky. The certificated private pilot and three passengers were not injured. Visual meteorological conditions prevailed and an instrument flight rules flight plan was filed for the personal flight that was conducted under the provisions of 14 Code of Federal Regulations Part 91.

The airplane was on approach to runway 24, a 4,326-foot-long, 75-foot-wide, asphalt, runway.

According to a Federal Aviation Administration (FAA) inspector, the pilot reported that the airplane was high and he utilized a steep descent to approach the runway. The airplane touched down on the runway, and bounced. The left landing gear collapsed, and the airplane veered off the left side of the runway, where it struck a taxiway sign, and sustained substantial damage to its fuselage and both wings.

The pilot did not report experiencing any mechanical malfunctions when interviewed by an FAA inspector after the accident. In a written statement, he subsequently reported that he performed a rapid turn and descent to the runway after the airplane was cleared for a left base to final approach. The pilot further stated that the engine did not respond to a throttle control input after the airplane bounced, and he was not certain if he experienced any mechanical malfunctions.

The airplane was equipped with a Lycoming IO-540 series, 300-horsepower engine.

Subsequent examination of the airframe and engine by an FAA inspector did not reveal any mechanical abnormalities. The engine was rotated by hand via the propeller, which remained attached and displayed curled tips on both blades. Thumb compression was attained on all cylinders and spark was observed at all spark plug ignition leads. Examination of the throttle and mixture controls did not reveal any discrepancies, and fuel flow was observed from all fuel injector lines when the boost pump was activated.

The airplane had been operated for about 20 hours since its most recent annual inspection, which was performed on February 24, 2011.

The pilot reported 3,800 hours of total flight experience, which included 3,600 hours in the same make and model as the accident airplane.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA11LA386