N340BG

Substantial
None

CESSNA 340AS/N: 340A-0068

Accident Details

Date
Wednesday, June 1, 2011
NTSB Number
WPR11LA363
Location
Fullerton, CA
Event ID
20110803X75301
Coordinates
33.871944, -117.979721
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's inability to maintain directional control during landing due to the left brake's degraded performance due to oil contamination, which resulted from the fatigue failure of an oil line component.

Aircraft Information

Registration
N340BG
Make
CESSNA
Serial Number
340A-0068
Engine Type
Reciprocating
Year Built
1976
Model / ICAO
340AC340
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
HUMANITARIAN AIRLIFT INTERNATIONAL
Address
31935 VIA FAISAN
Status
Deregistered
City
COTO DE CAZA
State / Zip Code
CA 92679-4133
Country
United States

Analysis

On June 1, 2011, about 1640 Pacific daylight time, a Cessna 340A, N340BG, was substantially damaged when its nose gear collapsed and deformed primary airframe structure in the wheel well. The event occurred when the pilot lost directional control as he taxied off runway 24 following an uneventful landing at the Fullerton Municipal Airport (FUL), Fullerton, California. Neither the airline transport certificated pilot nor passenger was injured. The airplane was registered to and operated by Humanitarian Airlift International, Coto de Caza, California. The personal flight was performed under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed, and no flight plan was filed. The airplane departed Riverside, California, about 1545. According to the pilot, following completion of maintenance he took off to reposition the airplane. No evidence of mechanical anomalies were noted, and his landing at FUL was normal. Near the completion of the landing rollout, with normal and effective breaking, the pilot initiated a turn off the runway. During this event, the left brake system failed, and the airplane veered into soft dirt adjacent to the runway. The nose wheel dug into the dirt and collapsed.

During the airplane's subsequent examination by an airframe and powerplant mechanic, a broken weld was found in the left engine's oil return line. The weld was located adjacent to the line's outlet nipple at the rear engine case. The line was routed to the case from the vacuum pump air-oil separator. Leaking oil from this broken weld had coated the rear engine case and left main landing gear brake assembly. According to the mechanic, engine oil on the left gear and wheel/ brake assembly caused braking action on the left brake to be reduced to zero. The weld break appeared related to fatigue.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR11LA363