Summary
On March 21, 2012, a Beech V35B (N17MJ) was involved in an incident near Malvern, AR. All 2 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot did not fly a stabilized approach and elected not to perform a go-around, which resulted in a runway excursion.
The pilot reported that he diverted to the accident airport due to weather with low ceilings. He encountered a gust of wind and rain during the turn from the base leg to final which caused him to be right of the runway centerline. Although the airplane floated down the runway and landed long, the pilot elected not to do a go-around. The pilot reported that the wet runway caused the tires to hydroplane, which increased the stopping distance. The airplane was traveling about 5 to 10 mph when it overran the end of the runway. The pilot attempted to veer the airplane to the left, but the right wing hit a fence and the nose gear collapsed. The examination of the airplane revealed substantial damage to a longeron in the empennage.
This incident is documented in NTSB report CEN12CA225. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N17MJ.
Accident Details
Probable Cause and Findings
The pilot did not fly a stabilized approach and elected not to perform a go-around, which resulted in a runway excursion.
Aircraft Information
Registered Owner (Historical)
Analysis
The pilot reported that he diverted to the accident airport due to weather with low ceilings. He encountered a gust of wind and rain during the turn from the base leg to final which caused him to be right of the runway centerline. Although the airplane floated down the runway and landed long, the pilot elected not to do a go-around. The pilot reported that the wet runway caused the tires to hydroplane, which increased the stopping distance. The airplane was traveling about 5 to 10 mph when it overran the end of the runway. The pilot attempted to veer the airplane to the left, but the right wing hit a fence and the nose gear collapsed. The examination of the airplane revealed substantial damage to a longeron in the empennage. The pilot reported that there was no mechanical malfunction or failure of the airplane.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN12CA225