N1178L

Substantial
None

CESSNA LC41-550FGS/N: 411101

Accident Details

Date
Wednesday, April 4, 2012
NTSB Number
CEN12LA234
Location
Telluride, CO
Event ID
20120409X20609
Coordinates
37.953887, -107.908889
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
4
Total Aboard
4

Probable Cause and Findings

The pilot's decision to land with a direct tailwind, which resulted in a loss of directional control, and his subsequent decision to attempt a go-around so late in the landing roll, which resulted in a stall.

Aircraft Information

Registration
N1178L
Make
CESSNA
Serial Number
411101
Engine Type
Turbo-jet
Model / ICAO
LC41-550FGC550
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
CLEARY EDWARD W
Address
825 N LAMB BLVD SPC 302
Status
Deregistered
City
LAS VEGAS
State / Zip Code
NV 89110-2349
Country
United States

Analysis

On April 4, 2012, at 1340 mountain daylight time, a Cessna Corvalis LC41-550FG, N1178L, registered to Performance by Design of Tuscon, Arizona, sustained substantial damage when it veered off runway 09 after landing at the Telluride Municipal Airport (TEX), Telluride, Colorado. The private pilot and his three passengers were not injured. Visual meteorological conditions prevailed and no flight plan was filed for the personal flight operated under the provisions of 14 Code of Federal Regulations Part 91. The flight originated at 1200 from Flagstaff, Arizona, and Telluride was its destination.

After an uneventful cross country flight, the pilot announced his intention to enter a right base for runway 9, even though there was a slight tailwind. He said that he had studied the airport the night before and felt that runway 9 was the best approach and landing for the field even with a slight tailwind.

The pilot stated that after crossing over the numbers, the airplane floated longer than he anticipated and touched down just before the 3,000 foot marker. The touchdown was straight and centered. The pilot felt comfortable that he had plenty of runway to safely bring the airplane to a stop and was expecting a smooth and straight rollout. Soon after touchdown, the airplane pulled to the left and the pilot responded by applying brakes with more pressure on the right brake. The airplane corrected slightly, so he eased off the brakes. The airplane was still pulling left so he repeated the process of right dominated braking but the airplane continued to pull left. At this point, the pilot realized that he was not going to be able to keep the airplane on the runway. He considered locking the brakes up and riding it out but felt that he could execute a go-around. As the pilot advanced the throttle and eased back on the control stick, the engine did not respond. The airplane nosed up, stalled, and came down off the left side of the runway. The pilot and all 3 passengers exited the airplane uninjured.

The reported wind at TEX about 5 minutes prior to the accident was from 270 at 12 knots, gusting to 16 knots.

METAR

KTEX 041935Z AUTO 27012G16KT 10SM CLR 10/M09 A3005 RMK AO2

FAA inspection of the airplane at the airport confirmed substantial damage to the integral composite main spars. Additionally, all three landing gear had sheared from the airplane during the accident sequence. Examination of the flight controls and brake system did not show any preexisting mechanical malfunction or abnormalities.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN12LA234