N28WF

Substantial
Minor

CESSNA 177AS/N: 17700876

Accident Details

Date
Tuesday, May 8, 2012
NTSB Number
WPR12LA198
Location
Hanksville, UT
Event ID
20120509X45351
Coordinates
38.568611, -110.957221
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot’s failure to maintain adequate airspeed while maneuvering at a low altitude in high density altitude conditions, which resulted in the airplane’s inability to climb or maintain clearance from terrain.

Aircraft Information

Registration
N28WF
Make
CESSNA
Serial Number
17700876
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
177AC177
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
AME HIGH LLC
Address
1220 N MAIN ST STE 5
Status
Deregistered
City
SPRINGVILLE
State / Zip Code
UT 84663-4025
Country
United States

Analysis

On May 8, 2012, about 1045 mountain daylight time, a Cessna 177A, N28WF, was substantially damaged when it impacted terrain while maneuvering at low altitude near Hidden Splendor Airfield (U660; elevation 4,821 feet), Hanksville, Utah. The commercial pilot and his passenger received minor injuries. The airplane was being operated by AME High LLC under the provisions of 14 Code of Federal Regulations Part 91. No flight plan had been filed for the local flight, which had originated from Spanish Fork, Utah, about 1 hour before the accident. Visual meteorological conditions prevailed.

About 1 hour into the flight, the pilot made a low pass over a remote airstrip descending to an altitude of about 25 feet above ground level and then applying power to climb back to cruise altitude. He said that the engine responded normally. However, approximately 15 seconds later, as the pilot raised the flaps, the airplane’s airspeed began to slow down, and the airplane stopped climbing. The pilot said he pushed the yoke in to lower the nose, but the airspeed did not increase. With the throttle all the way in and the mixture slightly leaned, the airplane began to descend. At that point the pilot found himself in a canyon and believing that the airplane would not climb, he selected an open sandy area and performed a forced landing. The nose wheel dug into the soft terrain, the nose landing gear separated, and the main landing gear collapsed. The airplane’s fuselage was bent and wrinkled, and the bottom of the forward section of the fuselage was crushed and buckled. The fuel lines around the fuel selector and the fuel shut off valve were compromised.

When the pilot contacted the aircraft salvage team for recovery, he stated that one wing fuel tank was empty and the other had 12 gallons in it. After the pilot left the scene, some hikers reported placing vice grips on one of the fuel lines to stop an observed fuel leak. When the salvage team arrived at the accident site several days later, they reported finding no fuel in the left tank and 1/3 gallon in the right tank. The fuel selector was found on the right tank, but the fuel shut off valve was closed. They reported that both wings were undamaged, and the wing flaps were in the up position. They reported separating the engine from the airframe to facilitate its recovery from the bottom of the canyon.

On May 23, 2012, two Federal Aviation Administration inspectors examined the recovered wreckage. Their examination of the engine revealed no evidence of any preimpact mechanical malfunctions or failures that would have prevented its normal operation. When they examined and disassembled the carburetor, no fuel was found. During disassembly of the engine driven fuel pump, evidence of fuel was observed on the diaphragms and check valves. Using a temperature of 60 degrees Fahrenheit, the density altitude at the accident site was calculated to be 6,000 feet, and at this density altitude, the normally aspirated 150-horsepower engine would have been capable of producing 120 horsepower.

The pilot reported that on his departure from Spanish Fork, the airplane had full fuel tanks or 48 gallons of useable fuel on board. The manufacturer’s “Owner’s Manual” for the 1968 model airplane indicates a fuel burn rate in cruise flight of between 8 and 9 gallons per hour.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR12LA198