N74914

Substantial
None

HUGHES TH-55S/N: 67-15442

Accident Details

Date
Saturday, May 19, 2012
NTSB Number
ERA12CA357
Location
Pittsfield, PA
Event ID
20120524X84631
Coordinates
41.826389, -79.361389
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The student pilot's failure to maintain helicopter control during an encounter with loss of tail rotor effectiveness.

Aircraft Information

Registration
Make
HUGHES
Serial Number
67-15442
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
TH-55
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
2
FAA Model
TH-55

Registered Owner (Current)

Name
TACHOIR STEVEN E
Address
977 WATSON FARM RD
City
MARIENVILLE
State / Zip Code
PA 16239-6127
Country
United States

Analysis

According to the student pilot, he had completed a solo flight earlier in the day that included 7 takeoffs and landings. After refueling, he completed a local flight and returned to the departure airport where he initiated an approach to the runway with a 7-knot, left quartering tailwind. The approach terminated "perfectly" to a normal hover. According to the pilot, the helicopter "started spinning to the right" and the spin could not be arrested with full application of left pedal. The pilot stated he then increased collective pitch and the corresponding increase in engine power aggravated the spin. He then attempted a hovering autorotation, but the helicopter landed hard, rolled over on to its side, and was substantially damaged. A witness described the helicopter as it approached "flying somewhat erratically" about 40 feet above the runway. The helicopter was "twisting" to the left and right as it hovered "shakily" closer to the runway. The helicopter noise increased, the nose pitched up, the main rotors struck the ground, and the helicopter came to rest on its side. An FAA advisory circular stated that loss of tail rotor effectiveness (LTE) was a critical, low-speed aerodynamic flight characteristic which could result in an uncommanded rapid yaw rate which does not subside of its own accord and, if not corrected, could result in the loss of aircraft control. Further, any maneuver which required the pilot to operate in a high-power, low-airspeed environment with a left crosswind or tailwind created an environment where unanticipated right yaw may occur. The pilot reported 40 total hours of flight experience, all of which was in the accident helicopter make and model. A detailed examination of the wreckage by Federal Aviation Administration inspectors revealed no pre-impact mechanical anomalies.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA12CA357