N379SW

MINR
None

BOEING 737-3H4S/N: 26586

Accident Details

Date
Friday, July 27, 2012
NTSB Number
DCA12IA113
Location
El Paso, TX
Event ID
20120727X13551
Coordinates
31.807222, -106.376388
Aircraft Damage
MINR
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
76
Total Aboard
76

Probable Cause and Findings

the rupture of the nose landing gear hydraulic line that resulted from abrasions due to contact with the nose landing gear tire. Contributing to the incident was the incorrect installation of union and restrictor on the actuator.

Aircraft Information

Registration
N379SW
Make
BOEING
Serial Number
26586
Year Built
1994
Model / ICAO
737-3H4

Registered Owner (Historical)

Name
SOUTHWEST AIRLINES CO
Address
2702 LOVE FIELD DR # HDQ-4GC
Status
Deregistered
City
DALLAS
State / Zip Code
TX 75235-1908
Country
United States

Analysis

HISTORY OF FLIGHT

On July 27, 2012, about 1400 mountain daylight time (MDT), Southwest Airlines flight 1871, a Boeing 737-3H4, N379SW, experienced a structural failure of the nose gear actuator retract beam when the landing gear was selected down during approach to El Paso International Airport (KELP), El Paso, Texas. There were no injuries to the 71 passengers and 5 crewmembers on board and the airplane sustained minor damage. The flight was operating under the provisions of Title 14 Code of Federal Regulations (CFR) Part 121 on a regularly scheduled passenger flight from Las Vegas McCarran International Airport (KLAS), Las Vegas, Nevada to KELP. Visual meteorological conditions prevailed at the time of the incident.

The captain was the pilot flying and the first officer was the pilot monitoring.

At 1400:37, after receiving a clearance from Air Traffic Control (ATC) for a visual approach to runway 8R, the captain asked for "landing gear down".

At 1400:40, as the landing gear was extended; two loud snapping sounds were heard (later described by the captain as "a very loud bang." The captain and first officer discussed the sound and expressed concern regarding the condition of the nose gear.

At 1401:17, the first officer requested a fly-by from the tower and asked that the tower controller inspect the nose gear. The captain then briefed the fly-by and go-around procedure with the first officer. The crew conducted a fly-by at 500 feet above ground level.

At 1404:32, the tower controller advised the flight crew that the nose gear appeared normal and the crew entered a right traffic pattern for a visual approach to runway 8R.

The flight crew conducted a visual approach and landing on runway 8R, and then taxied to the gate uneventfully. During the post flight inspection, the flight crew discovered a puddle of hydraulic fluid under the nose gear and then found the A hydraulic system quantity reduced.

Further inspection by maintenance personnel revealed damage to a hydraulic hose and the nose gear actuator retract beam.

INJURIES TO PERSONS

There were no injuries to the 71 passengers and 5 crewmembers.

DAMAGE TO AIRPLANE

The lower T chord of the actuator retract beam was fractured across the horizontal leg of the T chord and into the radius of the vertical leg about 16 inches aft of the nose wheel forward bulkhead.

The nose gear actuator retract beam was comprised of 4 individual web bays each separated by a vertical web stiffener. The bays were numbered 1 thru 4 beginning with the aft most bay. The aft most bay, bay 1, was undamaged. Bay 2 was buckled along a 45-degree angle forward and down from the aft upper fastener. Bay 3 was also buckled along a 45-degree angle forward and down from the aft upper fastener. The vertical stiffener was cracked vertically along the radius at the lower fastener.

A gap of about 3/8 of an inch was also present between the lower portion of the stiffener and the web. The entire lower edge of the web in Bay 4 was displaced outboard to the left consistent with the lower T chord displacement with no other obvious signs of damage. The lower T chord was displaced outboard and to the left by as much as 2 inches at STA 243.7 in the area of the lower T chord fracture.

All the examined fracture surfaces exhibited features consistent with overstress failures with no evidence of fatigue.

The nose landing gear (NLG) retract actuator hydraulic line was ruptured about 8.5 inches from the forward end of the hose (the end connected to the airplane.) In the area of the rupture, 3.18 inches of black outer spiral wrap was missing. Abrasion marks were also evident on the corrosion resistant steel (CRES) braid on the outboard side, facing away from the actuator beam, also aligned with the axis of the hose. Individual CRES strands were broken with the free ends abraded down to "chisel points" in numerous locations. The Teflon inner liner was ruptured in the area of the damaged CRES braid.

PERSONNEL INFORMATION

The captain, age 47, held a valid FAA Airline Transport Pilot (ATP) certificate with a B737 type rating and a current FAA first-class medical certificate with a limitation requiring him to possess glasses to correct for near vision. The captain reported approximately 15,110 hours total time including about 7,500 hours pilot-in-command and 9,960 hours on the B-737.

The first officer, age 36, held a valid FAA ATP certificate with type ratings for ATR-42, ATR-72, EMB-135, EMB-145, and B737, and a current FAA first-class medical certificate with no limitations. The first officer reported 9,500 hours total time at the time of the incident.

AIRCRAFT INFORMATION

The incident airplane, manufacturer serial number 26586, is a Boeing B737-3H4 equipped with two CFM International CFM56-3B2 turbofan engines. Records indicate the airplane was delivered in 1994.

The airplane had logged about 59,939 hours total time on the airframe and 49,780 cycles as of the day of the incident, and the most recent inspection was conducted on November 5, 2011, as part of the operator's continuous airworthiness maintenance program.

METEOROLOGICAL INFORMATION

The aviation routine weather report (METAR) recorded at 1951 at ELP, indicated wind from 110 degrees at 16 knots gusting to 23 knots, visibility 10 statute miles, few clouds at 5,500 feet, scattered clouds at 10,000 feet, broken cloud layers at 15,000 feet and 25,000 feet, temperature 29 degrees Celsius, dewpoint temperature 16 degrees Celsius, altimeter setting 30.09 inches mercury.

AIRPORT INFORMATION

El Paso International Airport is located 4 miles northeast of El Paso, TX at an elevation of 3,962 feet above mean sea level. The airport has six runways. The landing runway, runway 8R, is grooved asphalt 150 feet wide and 9,028 feet long with a runway end elevation of 3,927 feet above mean sea level. The runway is served by a 4-light precision approach path indicator with a 3-degree glideslope on the left side of the runway and runway end identifier lights.

FLIGHT RECORDERS

The cockpit voice recorder (CVR), an Allied Signal Model 6022, serial number 2319, was removed from the airplane and downloaded at the NTSB Vehicle Recorder Laboratory. The cockpit voice recorder contained 2 hours, 5 minutes of recording on two sets of audio data files; a 2-channel recording containing the last 2 hours of recorded data and a 4-channel file containing the last 30 minutes of recorded data. The audio quality of the channels containing information from the captain's and first officer's audio panels, and the audio quality of the channel containing information from the cockpit area microphone was characterized as good. The recording included events from the flight beginning with the departure climb out prior to reaching 10,000 feet and ending when the CVR was deactivated about 40 minutes after landing. Timing on the CVR summary was established by correlating CVR elapsed time to common events on the Flight Data Recorder (FDR) and adjusting to local MDT.

The FDR, an Allied Signal Model 6022, serial number 0832, was removed from the airplane and downloaded at the NTSB Vehicle Recorder Laboratory. The recorder arrived in good condition and contained approximately 27.2 hours of data which was extracted normally. The event flight was the last flight of the recording and its duration was approximately 1 hour and 37 minutes. Correlation of the FDR data to event local time, MDT, was established using the recorded GMT (Greenwich Mean Time) parameter.

TESTS AND RESEARCH

SYSTEMS

The NLG hydraulic hose, transfer cylinder, retract actuator and hydraulic modular package assemblies were removed from the airplane for examination.

Visual examination of the hydraulic hose revealed a rupture of the hose located 8.5 inches from the "A" end of the hose (the end attached to the airplane, opposite the end attached to the actuator) and approximately 3.18 inches of the black outer spiral wrap was missing in this area. The ends of the spiral wrap showed abrasion aligned with the axis of the hose on the outboard side away from the actuator beam and an arc shape was evident. Abrasion marks were also found on the corrosion resistant steel (CRES) braid with individual strands of the CRES broken and some ends worn down and some strands bent over facing forward. The Teflon inner liner was ruptured in the area of the damaged CRES and black debris were found in and around the damaged CRES braids.

A visual examination of the transfer cylinder indicated no signs of damage or defects except that a tab on the identification tag was broken. Leakage and operational tests were conducted in accordance with the Component Maintenance Manual (CMM) and no faults were found.

A visual examination and a digital radiography inspection of the retract actuator was conducted with no anomalies noted. A functional test of the actuator was conducted in accordance with the CMM. The actuator appeared to operate normally during 5 complete extend and retract cycles with snubbing apparent at both ends of the stroke and no leaks noted.

Additional leak testing was accomplished by extending the actuator as it would be in the gear retracted position and removing hydraulic pressure. When the gear extend hose fitting was removed to simulate a ruptured hydraulic hose, leakage started as a drip and progressed to a steady stream.

Disassembly of the actuator revealed the restrictor fitting was installed in the head end of the actuator and the union fitting was installed on the rod end cap. The engineering drawing, the CMM, and the Illustrated Parts Catalogue require the restrictor fitting to be installed in the rod end cap and the union fitting to be installed in the head end.

The hydraulic modular package assembly was visually examined with no defects noted. The assembly was functionally tested in accordance with the CMM with no faults found during the ten elements of the test procedure.

NLG Functio...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DCA12IA113