N1356Y

Substantial
None

BARNEY STARDUSTRER SA-100S/N: B-1

Accident Details

Date
Monday, September 17, 2012
NTSB Number
WPR12LA423
Location
Chandler, AZ
Event ID
20120918X81545
Coordinates
33.268890, -111.811111
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A loss of engine power as a result of fuel exhaustion due to a fuel line failure. Contributing to the accident was the pilot’s failure to adhere to the maintenance inspection criteria for the airplane.

Aircraft Information

Registration
Make
BARNEY
Serial Number
B-1
Engine Type
Reciprocating
Model / ICAO
STARDUSTRER SA-100
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
STARDUSTER SA-100

Registered Owner (Current)

Name
BOGGS JOHN D
Address
203 N 31ST ST
City
DUNCAN
State / Zip Code
OK 73533-2439
Country
United States

Analysis

On September 17, 2012, about 0954 mountain standard time, an experimental amateur-built Barney Starduster SA-100 airplane, N1356Y, sustained substantial damage following a loss of engine power and subsequent hard landing at the Chandler Municipal Airport (CHD), Chandler, Arizona. The private pilot, the sole occupant of the airplane, was not injured. The airplane was registered to the pilot, and operated as a visual flight rules flight under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed and no flight plan was filed for the flight that originated from Casa Grande, Arizona, about 14 minutes before the accident.

In a written statement to the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), the pilot reported that the engine stopped developing power as he entered the airport traffic pattern at CHD. The pilot initiated a forced landing in an open area adjacent to runway 22L and landed hard.

Postaccident examination of the airplane by a representative of the FAA revealed structural damage to the right wing and fuselage.

The pilot reported that postaccident examination of the airplane revealed that the Number 4 steel braided fuel line that supplies fuel from the fuel pump to the fuel pressure sending unit, lost "integrity." The pilot estimated that he lost about 3.5 gallons of fuel during the 14-minute flight; the airplane subsequently lost engine power about 3 minutes before landing.

The pilot stated that he departed Casa Grande with about 6 gallons of fuel onboard, and estimated that the flight would require about 2 gallons of fuel. The airplane's digital fuel totalizer showed about 4.2 gallons of fuel remaining within the main fuel tank after the accident; however, examination of the fuel tank (not breached) showed less than one gallon of total fuel remaining.

The airplane's most recent conditional inspection was completed on May 11, 2011, about 16 months prior to the accident. Review of the operation limitations for the airplane revealed that item 12 states in part "…no person shall operate this aircraft unless within the preceding 12 calendar months it has had a condition inspection performed in accordance with Appendix D of Part 43 and found to be in a condition for safe operation."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR12LA423