N172HACESSNA 172M2012-09-19 NTSB Accident Report

Substantial
Serious

CESSNA 172MS/N: 17260872

Summary

On September 19, 2012, a Cessna 172M (N172HA) was involved in an accident near Quitman, MS. The accident resulted in 1 serious injury. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this accident to be: The pilot’s improper preflight inspection, which resulted in a total loss of engine power due to fuel exhaustion.

The pilot was performing a routine pipeline patrol flight at 1,500 feet agl, and after flying for about 3 hours, the engine “sputtered,” then ceased producing power. The pilot then attempted to restart the engine, but was unsuccessful, and prepared for an emergency landing in a farm field below. The pilot was unable to recall the events that subsequently transpired, but a post-accident examination of the airplane showed that the left main landing gear collapsed during the landing, resulting in substantial damage to the left wing and engine firewall. Additionally, the fuel system remained intact and both fuel tanks were absent of fuel. About 1/2-pint of fuel was recovered from the fuel strainer, carburetor supply fuel line, and the carburetor float bowl.

This accident is documented in NTSB report ERA12CA568. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N172HA.

Accident Details

Date
Wednesday, September 19, 2012
NTSB Number
ERA12CA568
Location
Quitman, MS
Event ID
20120920X92813
Coordinates
32.040000, -88.728057
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot’s improper preflight inspection, which resulted in a total loss of engine power due to fuel exhaustion.

Aircraft Information

Registration
Make
CESSNA
Serial Number
17260872
Engine Type
Reciprocating
Model / ICAO
172MC172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MCCALL FREDDIE W
Address
PO BOX 2334
Status
Deregistered
City
BREWTON
State / Zip Code
AL 36427-2334
Country
United States

Analysis

The pilot was performing a routine pipeline patrol flight at 1,500 feet agl, and after flying for about 3 hours, the engine “sputtered,” then ceased producing power. The pilot then attempted to restart the engine, but was unsuccessful, and prepared for an emergency landing in a farm field below. The pilot was unable to recall the events that subsequently transpired, but a post-accident examination of the airplane showed that the left main landing gear collapsed during the landing, resulting in substantial damage to the left wing and engine firewall. Additionally, the fuel system remained intact and both fuel tanks were absent of fuel. About 1/2-pint of fuel was recovered from the fuel strainer, carburetor supply fuel line, and the carburetor float bowl. Following the accident, the pilot stated that he did not check the fuel level prior to departing on the accident flight, and that the accident could have been prevented by performing a proper preflight inspection of the airplane using the publish procedure in the pilot’s operating handbook and not “repetitive memory.”

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA12CA568