N234RHHENRIE RAYMOND ZENITH CH 701 STOL2012-09-29 NTSB Accident Report

Substantial
Minor

HENRIE RAYMOND ZENITH CH 701 STOLS/N: 7-6049

Summary

On September 29, 2012, a Henrie Raymond ZENITH CH 701 STOL (N234RH) was involved in an accident near Ashland, MS. The accident resulted in 2 minor injuries. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this accident to be: The pilot’s inadequate compensation for crosswind conditions during initial climb, which resulted in an impact with trees and terrain.

The pilot was attempting to depart the airport to return home in the experimental light sport aircraft. According to the pilot’s statement, just before takeoff, he noted that the windsock was “still” and initiated his takeoff roll. About 20 feet above ground level (agl), the flight encountered a left crosswind causing the airplane to go to the right. He corrected by immediately applying left aileron and left rudder control inputs, then removed the aileron and rudder control inputs. The flight continued and about 30 feet agl, the flight encountered another wind gust that pushed the airplane to the right “faster” than he could apply corrections.

This accident is documented in NTSB report ERA12CA588. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N234RH.

Accident Details

Date
Saturday, September 29, 2012
NTSB Number
ERA12CA588
Location
Ashland, MS
Event ID
20121003X52835
Coordinates
34.808334, -89.193054
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot’s inadequate compensation for crosswind conditions during initial climb, which resulted in an impact with trees and terrain.

Aircraft Information

Registration
Make
HENRIE RAYMOND
Serial Number
7-6049
Year Built
2010
Model / ICAO
ZENITH CH 701 STOL

Registered Owner (Historical)

Name
HENRIE RAYMOND
Address
3968 LURAY RD
Status
Deregistered
City
BEECH BLUFF
State / Zip Code
TN 38313-7636
Country
United States

Analysis

The pilot was attempting to depart the airport to return home in the experimental light sport aircraft. According to the pilot’s statement, just before takeoff, he noted that the windsock was “still” and initiated his takeoff roll. About 20 feet above ground level (agl), the flight encountered a left crosswind causing the airplane to go to the right. He corrected by immediately applying left aileron and left rudder control inputs, then removed the aileron and rudder control inputs. The flight continued and about 30 feet agl, the flight encountered another wind gust that pushed the airplane to the right “faster” than he could apply corrections. The right wingtip impacted a treetop causing the airplane to reverse its direction, descend rapidly, and impact the ground causing structural damage to the wings and fuselage. The pilot reported no preimpact mechanical failures or malfunctions. A representative of the airplane designer reported to NTSB that a 10 knot crosswind is well within the airplane’s maximum demonstrated crosswind limitation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA12CA588