Accident Details
Probable Cause and Findings
A total loss of engine power after the failure of the No. 4 connecting rod due to oil starvation, which resulted in a subsequent forced landing. Contributing to the accident was the pilot’s failure to clearly state that the aircraft had lost all power and the air traffic controllers’ incomplete understanding of the emergency, which resulted in the controllers vectoring the airplane too far from the airport to reach the runway.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHTOn January 4, 2013, about 1419 eastern standard time, a Beechcraft H35, N375B, owned and operated by a private individual, experienced a loss of engine power while in cruise flight and was destroyed when it impacted a house, while on approach to the Flagler County Airport (XFL), Palm Coast, Florida. The private pilot and two passengers were fatally injured. Instrument meteorological conditions prevailed and an en route instrument flight rules (IFR) clearance was obtained for the flight, which departed Saint Lucie County International Airport (FPR), Fort Pierce, Florida, and was destined for Knoxville Downtown Island Airport (DKX), Knoxville, Tennessee. The personal flight was conducted under the provisions of Title 14 Code of Federal Regulations Part 91.
The airplane arrived at FPR after flying from Stella Maris, Bahamas. The passengers cleared U.S. Customs about 1145. The airplane was subsequently refueled and departed for DKX under visual flight rules.
According to air traffic control information provided by the Federal Aviation Administration (FAA), the pilot contacted Daytona Approach control about 1407, and reported vibrations and an "oil pressure problem." The controller advised the pilot that the airports in the area were IFR with cloud ceilings of 900 to 1,000 feet above ground level. The pilot received radar vectors for an airport surveillance radar approach to runway 29 at XFL, which was about 8 miles north of the airplane's position. At 1411:06, the pilot reported that the engine oil pressure was "zero" with "cool cylinders." At that time, the airplane was flying at an altitude of 5,300 feet mean seal level (msl), and was located about 2.5 miles from the approach end of runway 11, at XFL. The airplane continued to be vectored to a point about 6.5 miles northeast of the airport and was provided headings to the south and then west, to the final approach course for runway 29. The airplane was subsequently cleared to land about 1416. Radar contact with the airplane was lost when the airplane was about 2 miles from the runway, at an altitude of 200 feet msl. At 1418:27, the pilot transmitted "…we need help; we're coming in with smoke." There were no further communications from the airplane.
The XFL airport director observed the airplane as it approached runway 29. He described the weather conditions as instrument meteorological conditions with a low ceiling and mist. He observed the airplane "break out" of the cloud layer, very low, just above the tree line. The airplane's wings were level as it descended and disappeared in the tree line.
Another witness, who was an airline transport pilot and flight instructor, reported that the airplane looked "slow" as it exited clouds, was in a nose high attitude, and appeared to "stall" prior to descending below the tree line, which was followed by smoke about 10 seconds later. PERSONNEL INFORMATIONThe pilot, age 58, held a private pilot certificate, with ratings for airplane single-engine land and instrument airplane. The pilot's logbooks were not recovered. His most recent FAA third class medical certificate was issued on December 31, 2012. At that time, he reported a total flight experience of 1,300 hours, which included 30 hours during the previous 6 months. The pilot reported 1,100 hours of total flight experience, with 50 hours during the previous 6 months, on an FAA medical certificate application dated February 4, 2010. AIRCRAFT INFORMATIONThe four-seat, all-metal, low-wing, retractable-gear airplane, serial number D-5121, was manufactured in 1957. It was powered by a Continental Motors IO-470-C1, 250-horsepower engine and equipped with a Beech 278 propeller assembly. According to Beechcraft, the airplane was originally manufactured with a Continental Motors O-470-G series engine, which could be modified post manufacturer with a fuel injected engine per Beech Kit 35-648, "Engine Conversion to Fuel Injection on the Beech Model H35 Bonanza." No documentation for the engine that was installed on the accident airplane was found.
The airplane was found to have been modified with the addition of 15-gallon fiberglass wingtip fuel tanks, which would have included a wingtip tank fuel transfer pump mounted in each respective wing's wheel-well, to allow fuel to be transferred from each wingtip fuel tank, to its respective wing. There was no record of a supplemental type certificate for the installation of wingtip fuel tanks found in the airplane's FAA airworthiness file.
According to FAA records, the pilot purchased the airplane on May 30, 2008.
The airplane's maintenance records were not located. According to an FAA inspector, it was reported that the pilot traveled with his personal logbook and the airplane's maintenance records onboard the airplane. Additional information obtained by the FAA inspector revealed that the engine's No. 1 and No. 4 cylinders were replaced due to low compression during early December 2012; however, no work orders or other associated documentation could be located.
A friend of the pilot reported that he believed that the airplane's last annual inspection was performed around September-October 2012. He stated that he was not aware of any previous engine issues with the airplane, except for a small oil leak.
In a written statement, the lineman who refueled the airplane at FPR reported that he noticed "visible oil leaks" on the airplane's nose gear strut. In addition, after he informed the pilot of a fuel imbalance prior to refueling, the pilot informed the lineman that the airplane's right fuel pump was not working. METEOROLOGICAL INFORMATIONThe weather reported at XFL at 1350 was: wind 360 degrees at 7 knots, visibility 3 statute miles, ceiling 900 feet broken, 1,400 feet overcast, temperature 15 degrees Celsius (C), dew point 13 degrees C, and altimeter 30.22 in/hg. AIRPORT INFORMATIONThe four-seat, all-metal, low-wing, retractable-gear airplane, serial number D-5121, was manufactured in 1957. It was powered by a Continental Motors IO-470-C1, 250-horsepower engine and equipped with a Beech 278 propeller assembly. According to Beechcraft, the airplane was originally manufactured with a Continental Motors O-470-G series engine, which could be modified post manufacturer with a fuel injected engine per Beech Kit 35-648, "Engine Conversion to Fuel Injection on the Beech Model H35 Bonanza." No documentation for the engine that was installed on the accident airplane was found.
The airplane was found to have been modified with the addition of 15-gallon fiberglass wingtip fuel tanks, which would have included a wingtip tank fuel transfer pump mounted in each respective wing's wheel-well, to allow fuel to be transferred from each wingtip fuel tank, to its respective wing. There was no record of a supplemental type certificate for the installation of wingtip fuel tanks found in the airplane's FAA airworthiness file.
According to FAA records, the pilot purchased the airplane on May 30, 2008.
The airplane's maintenance records were not located. According to an FAA inspector, it was reported that the pilot traveled with his personal logbook and the airplane's maintenance records onboard the airplane. Additional information obtained by the FAA inspector revealed that the engine's No. 1 and No. 4 cylinders were replaced due to low compression during early December 2012; however, no work orders or other associated documentation could be located.
A friend of the pilot reported that he believed that the airplane's last annual inspection was performed around September-October 2012. He stated that he was not aware of any previous engine issues with the airplane, except for a small oil leak.
In a written statement, the lineman who refueled the airplane at FPR reported that he noticed "visible oil leaks" on the airplane's nose gear strut. In addition, after he informed the pilot of a fuel imbalance prior to refueling, the pilot informed the lineman that the airplane's right fuel pump was not working. WRECKAGE AND IMPACT INFORMATIONThe airplane impacted trees and a residence about 3/4 mile from the approach end of runway 29, slightly left of the extended centerline. The initial impact point (IIP) was identified as a pine tree that was about 60 feet tall and contained broken limbs about 30 to 35 feet above ground level. Various components of wreckage extended from the IIP, on a heading of 288 degrees magnetic for 50 feet. The remainder of the airplane impacted the roof of a detached single family home and a large fire ensued, which destroyed most of the airplane and dwelling.
The airplane's left outboard wing, with about one-half of the corresponding aileron attached, displayed evidence of a tree strike and was found at the base of a tree located about 60 feet from the back of the house. The inbound portion of the left aileron was observed near the right wing, which was inverted and located along the back of the house. The empennage came to rest inverted on the backside edge of the roof alongside of a section of the right wing inboard leading edge. Other remains of the fuselage and left wing were found inside the house. Examination of the airplane's flight control cables did not reveal evidence of any preimpact failures. The right flap actuator remained intact and was observed in a flap retracted position. The landing gear actuator was not observed and the preaccident position of the landing gear could not be confirmed.
The engine was found inverted on the floor of the house. It sustained a significant amount of thermal and impact damage, which destroyed all accessories, with the exception of the propeller governor, which was intact, but fired damaged. A large hole was observed in the crankcase, which contained a portion of the No. 4 connecting rod. The engine was forwarded to Continental Motors Inc., Mobile, Alabama, for further examination.
The propeller remained attached to the crankshaft flange. The spinner was dented and did...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA13FA105