N342FS

Substantial
None

CESSNA 305AS/N: 21831

Accident Details

Date
Saturday, February 2, 2013
NTSB Number
WPR13LA112
Location
Camarillo, CA
Event ID
20130203X23237
Coordinates
34.213890, -119.094444
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A tailwheel vibration upon touchdown and the subsequent loss of directional control for reasons that could not be determined because postaccident examination revealed no mechanical malfunctions or failures that would have precluded normal operation. 

Aircraft Information

Registration
Make
CESSNA
Serial Number
21831
Engine Type
Reciprocating
Model / ICAO
305A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
305A

Registered Owner (Current)

Name
PETERSEN AIRCRAFT INC
Address
8090 HIGHWAY 40 NE
City
MURDOCK
State / Zip Code
MN 56271-8014
Country
United States

Analysis

On February 2, 2013, about 1400 Pacific standard time, a Cessna 305A, N342FS, experienced a runway excursion at Camarillo Airport, Camarillo, California. The pilot/owner was operating the airplane under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The commercial pilot and a pilot-rated passenger were not injured; the airplane sustained substantial damage. The local personal flight departed Camarillo at 1300. Visual meteorological (VMC) conditions prevailed, and no flight plan had been filed.The pilot reported that the preflight detected no anomalies with the airplane. The departure and local area flight had been uneventful. The three-point landing was normal in minimal wind. Immediately upon touchdown, the pilot felt an extreme tail wheel vibration, and the airplane abruptly made a sharp left turn. The airplane veered off the runway, and the right main landing gear collapsed. The right wing, right aileron, right landing gear box, horizontal stabilizer, and right elevator sustained substantial damage. The pilot noted that post flight inspection revealed that the right rudder cable had broken.

Examination by a Federal Aviation Administration inspector revealed that the rudder control cables for the front and back seats, which extend from the rudder pedals to the rudder control horn, had separated about 14 inches from the rudder pedals. This was in the vicinity of the collapsed right main gear attachment point. No observations were made that could account for the tail wheel vibration on touchdown.

The National Transportation Safety Board Materials Laboratory examined the rudder control cables. The specialist conducting the examination determined that both cable fractures were consistent with overstress; no evidence of preexisting defects, such as corrosion or fatigue, was found.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR13LA112