Accident Details
Probable Cause and Findings
The pilot's failure to maintain directional control of the airplane while landing, which resulted in a runway excursion.
Aircraft Information
Registered Owner (Historical)
Analysis
According to the pilot, the airplane was on a stabilized approach to runway 22 with right crosswind corrections in place. Upon touchdown, he heard a "squealing" noise and then the airplane veered to the left. He applied takeoff power in an attempt take off but the airplane continued left, exited the runway, and hit an embankment. Examination of the airplane by a Federal Aviation Administration (FAA) inspector revealed substantial damage to the right wing spar, inboard crushing of the right wing flap, and crushing of the engine firewall. Wheel brake continuity was verified by the FAA inspector. The FAA inspector also noted that there was no flat skid mark on the runway that is synonymous with a skidding tire. The pilot did not report any pre-impact mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA13CA202