N44GC

MINR
None

BEECH 58S/N: TH-453

Accident Details

Date
Saturday, May 4, 2013
NTSB Number
CEN13FA267
Location
Mena, AR
Event ID
20130509X40743
Coordinates
34.540554, -94.201385
Aircraft Damage
MINR
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A partial loss of power on both engines during takeoff for reasons that could not be determined because examination of the airframe and a test run of both engines revealed no mechanical anomalies that would have precluded normal operation.

Aircraft Information

Registration
N44GC
Make
BEECH
Serial Number
TH-453
Engine Type
Reciprocating
Year Built
1974
Model / ICAO
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
KEET MANAGEMENT CO
Address
2001 GREEN MOUNTAIN DR APT 110
Status
Deregistered
City
LITTLE ROCK
State / Zip Code
AR 72212-4504
Country
United States

Analysis

HISTORY OF FLIGHT

On May 4, 2013, at 1200 central daylight time, N44GC, a Beech 58 twin-engine airplane, sustained minor damage during a forced landing shortly after takeoff from the Mena Intermountain Municipal Airport (MEZ), Mena, Arkansas. The commercial pilot and the pilot rated passenger were not injured. The airplane was registered to and operated by the pilot rated passenger. Visual meteorological conditions prevailed and no flight plan was filed for the personal flight that was destined for the Bill and Hillary Clinton International Airport (LIT), Little Rock, Arkansas, under the provisions of 14 Code of Federal Regulations Part 91.

The pilot stated that the airplane just had the interior refurbished in Mena, Arkansas, and he and the owner were flying the airplane back to their home base in Little Rock. The owner was not current and had hired the pilot to fly the airplane back with him.

According to the pilot, he completed a preflight inspection before departure. He used the airplane's checklist to start the engines and both engines started immediately. The pilot taxied about 10-15 minutes to runway 27, where he performed an engine run-up on each engine using the checklist. The run-up was "normal" for each engine.

The pilot then lined the airplane up on the runway, applied "full power" to each engine, and departed. Once airborne, he initiated a right turn. The pilot said that when the airplane was about 1,200-1,400 feet, he brought the propeller levers back to 2,500 RPM and left the power on both engines at 30 inches Hg of manifold pressure (MP). Almost immediately after, the pilot heard a "faint" and indistinguishable "pop" from the left engine. Then both engines simultaneously went from "full power" to idle. The pilot was unable to maintain altitude and made an immediate turn back to runway 27.

The pilot said the mixture controls were full forward the entire flight. Each fuel tank was 3/4-full and the fuel selector was in the "on" position. The pilot said the MP gauge read 30 inches Hg and the fuel flow on the digital fuel gauge was "positive", about 25 gallons per hour per side. He did not recall looking at any of the other engine gauges because he was concentrating on making a safe landing.

The pilot landed the airplane gear-up on the grassy area just short of runway 27.

PERSONNEL INFORMATION

The pilot held a commercial pilot certificate for airplane single and multi-engine land, and instrument airplane. He also held a certified flight instructor certificate for airplane single and multi-engine land and instrument airplane. His last Federal Aviation Administration (FAA) first class medical certificate was issued on April 4, 2013, with no waivers or limitations. The pilot reported a total of 1,381 flight hours, of which 250 hours were in multi-engine airplanes and 32.6 of those hours were in a Beech 58. He also reported a total of 29 hours in a Beech 55.

AIRCRAFT INFORMATION

The airplane was a 1974 Beech 58 twin-engine airplane (serial number TH-453). The airplane had several modifications that were installed under specific FAA approved Supplemental Type Certificates (STC). These modifications included Continental Motors, Inc. IO-550-C engines, a 4-bladed Hartzell propeller, TurboGAMIjector fuel injectors and a Merlyn Products Inc. turbo-normalizing system.

An FAA approved airplane flight manual supplement was issued as a result of the Merlyn STC. A review of the supplement revealed an operating limitation for manifold pressure, which was not to exceed 30 inches. In addition, a placard had to be installed on the instrument panel. (This placard was found in the accident airplane above the manifold and fuel pressure gauges).

A review of the airplane's maintenance logbooks revealed the last 100-hour inspection was completed in April 2013 at an aircraft total time of 7,785.2 hours.

The left engine (serial number 684606) underwent a 100-hour inspection on April 11, 2013. At that time the engine had a total time of 973.3 hours and at the time of the accident it had a total of 974.2 hours.

The right engine (serial number 684609) underwent a 100-hour inspection on April 11, 2013. At that time the engine had a total time of 973.3 hours and at the time of the accident it had a total of 974.2 hours.

WRECKAGE EXAMINATION

On May 5, 2013, a Federal Aviation Administration (FAA) inspector performed a visual examination of the airplane. He reported that several propeller blades were damaged and there was some damage to the landing gear doors. No structural damage was noted. The inspector also sumped each fuel tank and the fuel was absent of debris and water.

The airplane, both engines, and the area where the airplane made the forced landing were examined May 29-30, 2013, by the National Transportation Safety Board (NTSB) Investigator-in-Charge (IIC). Also present for the examination were representatives from the Federal Aviation Administration (FAA), Continental Motors, Incorporated (CMI), Beechcraft Corporation, Hartzell Industries Inc., and Merlyn Products, Inc.

AIRFRAME

Examination of the airframe revealed the main entrance step had separated at the fuselage wall. The left elevator counter-balance horn was separated and the left elevator was buckled mid-span. The fuselage belly fairing that houses an air conditioning line was also separated. The fuselage belly skins exhibited evidence of minor buckling to internal structure. The nose landing gear doors were buckled. There was a small dent on the leading edge of the right wing just outboard of the engine.

Examination of the fuel system revealed no mechanical anomalies. The fuel selector had distinct detents in all positions and fuel flow was confirmed when the fuel selector was turned on and confirmed to stop flowing when turned to off. The operation of the boost pump (both hi/low) was confirmed when the engines were test run. Mid wing fuel sight gauges were examined. The left wing indicated less than 60 gallons of fuel, and the right wing indicated 55 gallons, which was adequate fuel to sustain flight. Both of the wing fuel tanks sump strainers were removed and were absent of debris.

RIGHT ENGINE

The 4-bladed Hartzell propeller was still installed on the engine and all four propeller blades were bent aft mid-span with some indications of twisting. There was leading edge to trailing edge scoring at the tips and span-wise scoring along the length of the bent section of the blades. Two blades exhibited leading edge gouging near the tip of blades. The propeller was removed from the engine and a 2-bladed constant speed/counter-weighted-fully feathering McCauley propeller was installed.

The top cowl had already been removed prior to the team's arrival, but the bottom cowl was still installed. The bottom cowl was removed. A crankshaft-propeller flange run-out was conducted and also checked for end-play. The test revealed no measurable results.

The top spark plugs were removed and appeared dark in color. The No.1 plug was black and carbon-fouled. The gaps also appeared very close. The top plugs were placed on a test bench and all produced normal spark. After the propeller was installed, a thumb compression check via manual rotation of the propeller was conducted. Compression was established on each cylinder.

LEFT ENGINE

The 4-bladed Hartzell propeller was still installed on the engine and all four propeller blades were bent aft mid-span with some indications of twisting. There was leading edge to trailing edge scoring at the tips and span-wise scoring along the length of the bent section of the blades. The propeller was removed from the engine and a 2-bladed constant speed/counter-weighted-fully feathering McCauley propeller was installed.

The top cowl had already been removed prior to the team's arrival, but the bottom cowl was still installed. The bottom cowl was removed. A crankshaft-propeller flange run-out was conducted and also checked for end-play. The test revealed no measurable results.

The top spark plugs were removed and appeared dark in color. The top plugs were placed on a test bench and all produced normal spark. After the propeller was installed a thumb compression check via manual rotation of the propeller was conducted. Compression was established on each cylinder.

ENGINE TEST-RUN

A calibrated 0-100 PSI gauge was installed on the left engine to measure metered fuel pressure at the outlet of the fuel transducer and fuel manifold. The airplane was then towed to a secure area on the airport where a dual engine run was conducted.

The left and right engines were started and warmed for approximately 6 minutes at idle (1000-1200 RPM) to allow the engines to achieve normal operating temperatures. Then the engines were shut down for a visual inspection of leaks. No leaks were noted. The engines were then re-started and brought to 1700 RPM and a magneto check was performed on each engine. Both magnetos checks were about 75 RPM drop, which was within limits. The propeller levers were then exercised from the full increase position toward a decrease position to the point where an RPM drop was detected. The lever was then placed back in the full increase position. The left throttle was then increased to an RPM of about 2650 RPM. The throttle was then advanced to the full throttle position (2700 RPM) and about 34 inches of manifold pressure was obtained (Both engines were equipped with a pressure relief valve, which maintains a maximum manifold pressure around 33 inches. It was not determined as to why the engines were able to achieve 34 inches of manifold pressure). Throttle position was then decreased to reach about 30 inches of manifold pressure. The throttle was then reduced to 1700 RPM. Then the right throttle was increased to obtain 2650 RPM and 30 inches of MP. Then both throttles were reduced to idle, and a 2 minute cool down was performed. Then each engine was secured by placing the fuel selector v...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN13FA267