N969BDPIPER PA-31-3502013-05-28 NTSB Accident Report

Substantial
None

PIPER PA-31-350S/N: 31-8152109

Summary

On May 28, 2013, a Piper PA-31-350 (N969BD) was involved in an incident near Page, AZ. All 5 people aboard were uninjured. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this incident to be: A loss of engine power during cruise flight due to fuel exhaustion. Contributing to the accident was the pilot's improper fuel planning.

The pilot stated that he and four passengers were about 4.5 hours into the flight and about 10 nm from their destination when the left low boost light illuminated. About 20 seconds later the left engine quit, and the pilot feathered the propeller. After about 1 minute the right low boost light illuminated, and 20 seconds later, the right engine quit. The pilot feathered the right propeller and proceeded to execute a forced landing in the desert 5 miles east of the intended destination. During the accident sequence the right engine separated from the airplane and the left wing buckled, resulting in substantial damage to the airplane.

This incident is documented in NTSB report WPR13CA245. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N969BD.

Accident Details

Date
Tuesday, May 28, 2013
NTSB Number
WPR13CA245
Location
Page, AZ
Event ID
20130528X22514
Coordinates
36.899166, -111.457221
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
5
Total Aboard
5

Probable Cause and Findings

A loss of engine power during cruise flight due to fuel exhaustion. Contributing to the accident was the pilot's improper fuel planning.

Aircraft Information

Registration
Make
PIPER
Serial Number
31-8152109
Engine Type
Reciprocating
Year Built
1981
Model / ICAO
PA-31-350PA31
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
AKN INC
Address
6000 DOUGLAS DR N
Status
Deregistered
City
CRYSTAL
State / Zip Code
MN 55429-2314
Country
United States

Analysis

The pilot stated that he and four passengers were about 4.5 hours into the flight and about 10 nm from their destination when the left low boost light illuminated. About 20 seconds later the left engine quit, and the pilot feathered the propeller. After about 1 minute the right low boost light illuminated, and 20 seconds later, the right engine quit. The pilot feathered the right propeller and proceeded to execute a forced landing in the desert 5 miles east of the intended destination. During the accident sequence the right engine separated from the airplane and the left wing buckled, resulting in substantial damage to the airplane. The pilot reported that the airplane had ran out of fuel, and that there were no preimpact mechanical failures or malfunctions that would have precluded normal operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR13CA245