N7643J

Substantial
None

WSK PZL MIELEC M-18BS/N: 1Z025-18

Accident Details

Date
Wednesday, July 3, 2013
NTSB Number
WPR13LA308
Location
Caldwell, ID
Event ID
20130705X70647
Coordinates
43.697498, -116.644447
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot’s improper decision to continue the takeoff with a tailwind after he recognized a performance problem with the airplane and his delayed action to dump the chemical load.

Aircraft Information

Registration
N7643J
Make
WSK PZL MIELEC
Serial Number
1Z025-18
Year Built
1984
Model / ICAO
M-18B

Registered Owner (Historical)

Name
VALLEY AIR SERVICE INC
Address
PO BOX 878
Status
Deregistered
City
CALDWELL
State / Zip Code
ID 83606-0878
Country
United States

Analysis

On July 3, 2013, about 0605 mountain daylight time, a WSK PZL Mielec M-18B (turbine-powered Dromader), N7643J, was substantially damaged during takeoff at Hubler Field Airport, Caldwell, Idaho. The commercial pilot, the sole occupant on board, was not injured. Valley Air Service, Inc., was operating the airplane under the provisions of 14 Code of Federal Regulations Part 137. Visual meteorological conditions prevailed for the local aerial application flight, which was originating at the time of the accident. A flight plan had not been filed.

The pilot stated that this was his first flight for the day, and he had approximately 490 gallons of applicant and 120 gallons of fuel on board. He taxied to the end of runway 29, a 2,800-foot-long runway and applied power for takeoff. The pilot said the airplane appeared to accelerate normally until the tail wheel came up and then the airplane's acceleration did not seem normal. He adjusted the power lever forward a bit, but the torque did not seem to increase. As he reached the end of the runway, he realized that he would not make it off the ground and that it was too late to abort. The pilot advanced the power lever all the way forward but the torque indication was only in the 80's percentile range. He pulled back on the control stick, and the main wheels left the ground, but the tail wheel felt like it was again on the ground.

The pilot jettisoned the applicant load, but the airplane struck a fence in a nose high attitude approximately 100 feet from the end of the runway. The airplane tumbled and came to rest in a river approximately 350 feet from the fence. The airplane's turbine engine separated from the airframe, and both wings exhibited aft accordion leading edge crushing.

The pilot stated that "a more prompt recognition of the problem and an earlier decision to dump the load [of applicant] may possibly have prevented the aircraft from hitting the fence."

The pilot reported that when he arrived at the airport at 0500 the wind was light and variable. At 0615 the reported wind at Caldwell Industrial Airport, Caldwell, located 3 nautical miles from the accident site was wind from 110 degrees at 8 knots.

During the postaccident examination, the Garrett AiResearch TPE331 turboshaft engine was removed from the accident scene and shipped to Honeywell Aerospace, Phoenix, Arizona. On August 1, 2013, a manufacturer's representative and a Federal Aviation Administration (FAA) inspector witnessed the disassembly of the engine. Additionally, the fuel control unit (FCU), propeller governor and P2T2 sensor were sent to Woodward, Inc., Rockford, Illinois, for examination under the supervision of an FAA inspector. At the conclusion of the examinations, no mechanical malfunctions or failures were found that would have precluded normal operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR13LA308