N2333Z

Substantial
Serious

BEECH 23S/N: M-49

Accident Details

Date
Thursday, July 18, 2013
NTSB Number
ERA13FA325
Location
Laurel, MD
Event ID
20130718X44907
Coordinates
39.089168, -76.824165
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot's inadequate preflight preparation of the airplane, which resulted in a total loss of engine power during takeoff and his decision to operate the unairworthy airplane.

Aircraft Information

Registration
N2333Z
Make
BEECH
Serial Number
M-49
Engine Type
Reciprocating
Year Built
1962
Model / ICAO
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
5010 EDMONDSON AVE
Status
Deregistered
City
BALTIMORE
State / Zip Code
MD 21229-2332
Country
United States

Analysis

HISTORY OF FLIGHTOn July 18, 2013, about 1011 eastern daylight time, a Beech 23, N2333Z, was substantially damaged after a loss of power when it struck a tree and then houses shortly after takeoff from Suburban Airport (W18), Laurel, Maryland. The private pilot was seriously injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight operated under the provisions of Title 14 Code of Federal Regulations Part 91, destined for Gettysburg Regional Airport (W05), Gettysburg, Pennsylvania.

According to the pilot, on the morning of the accident, he awoke about 0830, and left for the airport. He arrived at W18 at approximately 0910. He then preflighted the airplane and visually checked the fuel. It was full of fuel as he had topped it off two days before, and "everything was normal". He selected the left tank before taxi, and prior to departure did an engine runup, checking the engine for about 15 minutes. He did a "mag and mag drop" check and a "carb heat drop" check during the run-up and "both were normal".

Prior to departure he selected "one notch of flaps", and proceeded to takeoff from runway 03. Everything was normal until the airplane was over the end of the runway at approximately 250 feet when the engine suddenly lost power. The pilot switched tanks, and turned on the boost pump in an attempt to get the engine to run without result. He then maneuvered to the left, and then to the right. The last thing he remembered was seeing a gray house.

Review of air traffic control data revealed that the pilot had filed a VFR special flight rules area (SFRA) flight plan. Prior to departure, the pilot had obtained a beacon code to operate within the Washington SFRA however; he was not able to contact air traffic control prior to the loss of engine power. Radar data indicated that after takeoff, the airplane reached a peak altitude of 300 feet, but approximately 9 seconds later at 10:10:20, descended below the floor of radar coverage.

According to a witness, at approximately this time, she observed the airplane flying west to east and noticed the left wing "dropped" and the plane started heading towards the ground. She then heard a "boom" and observed smoke.

PERSONNEL INFORMATION

According to Federal Aviation Administration (FAA) records, the pilot held a private pilot certificate with ratings for airplane single-engine land, and instrument airplane. He also held a repairman experimental aircraft builder certificate. His most recent application for a FAA third-class medical certificate was dated July 19, 2006. The pilot reported that he had accrued 3,571 total hours of flight experience.

AIRCRAFT INFORMATION

The accident aircraft was a four place, low wing monoplane of conventional construction. The all metal semi-monocoque airframe structure was composed of aluminum, magnesium, and alloy steel. The wings were constructed of bonded aluminum honeycomb. It was equipped with tricycle landing gear, and was powered by a 160 horsepower, four cylinder, normally aspirated, air cooled engine, driving a two bladed, fixed-pitch, forged aluminum propeller.

According to the pilot, the airplane had been previously damaged prior to the accident, when it had been involved in an off airport landing in Wyoming in 1984 where the right main landing gear, wing box assembly, and right wing lower wing skins were damaged. Then in 1985 the rudder was replaced after it was damaged, and then most recently, the right wingtip had been hit by a lawnmower.

According to FAA and maintenance records the airplane was manufactured in 1962. The engine had been overhauled on January 1, 1992 at 4,476.44 total hours of operation. The airplane's most recent annual inspection was completed on January 5, 1998 at 4719.0 total hours of operation, and at the time of the accident, the airplane had accrued 4997.56 total hours of operation.

METEOROLOGICAL INFORMATION

The recorded weather at Tipton Airport (FME), Fort Meade, Maryland, located 3 nautical miles east of the accident site, at 1012, included: winds 360 at 3 knots, 10 miles visibility, sky clear, temperature 31 degrees C, dew point 22 degrees C, and an altimeter setting of 30.12 inches of mercury.

WRECKAGE AND IMPACT INFORMATION

Accident Site Examination

Post accident examination of the accident site revealed that the airplane had come to rest approximately a ½ mile from the departure end of runway 03. It initially made contact with a 40 foot tall pine tree, striking the tree approximately 24 feet above the base of the tree and fracturing the upper portion of the tree into two sections. The airplane then struck the northwest corner of a house separating the right wing from its mounting location. The airplane then continued forward approximately 70 feet, struck the west side of another house located across the street from the initial impact point with the tree, fracturing the fuselage just aft of the baggage door. It then came to rest against the southwest side of the residence with the left wing penetrating the front of the house.

Airplane Examination

Examination of the wreckage did not reveal any preimpact malfunctions of the airplane. There was no indication of structural failure and control continuity was established from the flight controls to the rudder pedals and control wheel. Further examination revealed that the right wingtip and right wing outboard leading edge displayed damage that had been taped over with duct tape and appeared to have occurred prior to the accident. The rudder was also a different color than the rest of the airplane.

Both wing tank fuel caps were closed and locked. Both the left and right wing fuel tanks were compromised however; approximately 12 ounces of fuel was recovered from left wing fuel tank. Examination of the fuel revealed that it was consistent with 100LL aviation gasoline, and a check with water finding paste revealed no indication of water being present.

Examination of the fuel strainer also revealed the presence of fuel consistent with 100LL aviation gasoline and a check with water finding paste also did not reveal the presence of water.

Examination of the cockpit revealed that the wing flap lever was in the 15 degree (first notch) position and the stabilator pitch trim was in the takeoff range (green arc). The fuel selector was in the right wing tank position. The primer was in and locked. The throttle was full open, the mixture was full rich, and the carburetor heat was off. The fuel boost pump was also off.

Propeller and Engine Examination

Examination of the propeller revealed that the propeller had remained attached to the crankshaft flange. One blade was curved aft about 10 degrees and exhibited chord-wise abrasions on the forward surface. The other blade was bent aft about 45 degrees at about mid-span. It exhibited chord-wise abrasions and paint transfer on the forward surface of the blade.

Examination of the engine revealed that it had remained attached to the aircraft firewall by the tubular engine mount. Examination of the engine revealed that the engine compartment contained the remains of bird nests, and bird excrement. A red colored piece of cloth was also visible inside the right cowling inlet. Further examination of the cloth revealed that it was the cloth jacketing from a foam filled cowl plug and that the cloth jacketing along with the foam insert were protruding from, and blocking, the engine combustion air inlet opening.

The drive train was rotated by turning the crankshaft flange and continuity of the crankshaft to the rear gears and to the valve train was confirmed. Suction and combustion were observed from all four engine cylinders.

The carburetor remained attached to the engine and no external damage was noted. The carburetor bowl screws were snug and no fuel stains were noted on the exterior surfaces of the carburetor. The carburetor was partially disassembled. Liquid with an odor consistent with that of aviation gasoline was observed in the carburetor bowl. A check with water finding paste revealed no indication of water in the bowl. No damage was noted to the carburetor internal components however, it was discovered that, a mud dauber wasp nest about the size of a golf ball was present in the carburetor throat (venturi) below the main fuel nozzle.

The engine driven fuel pump remained attached to the engine. It was removed and produced air at the outlet port when actuated by hand.

Both magnetos remained attached to the engine and produced spark from all ignition towers, and no damage was observed on the ignition harness. The electrodes on the No.1, 2, 3, and 4 sparkplugs from the top of the cylinders were undamaged and appeared normal. The No. 1 cylinder bottom spark plug was obstructed by the exhaust and was not removed. The No. 2, 3, and 4 cylinder bottom sparkplug electrodes, also were undamaged and appeared normal.

The starter had remained attached to the engine and displayed evidence of rotational scoring on the starter nose case. The generator had also remained attached to the engine and was undamaged.

The exhaust muffler displayed heavy rust deposits and circumferential cracking.

The engine contained about 6½ quarts of oil. The oil suction screen appeared clean, the inside of the oil filter appeared clean, the oil hoses to the oil cooler were secure, and oil cooler integrity was not compromised. According to the information recorded on the oil filter, the filter was last replaced on October 17, 2010 at 4995.26 total hours of operation.

TESTS AND RESEARCH

Additional Documents

Documents discovered in the wreckage revealed that some components on the airplane had either been worked on in the airplane or had been removed and replaced but had not been entered in to the aircraft logbook or engine logbook. These included the magnetos, attitude indicator, directional gyro, fuel filler caps, wingtips, and transponder.

Airplane Sale

According to the pilot the purp...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA13FA325