N27BD

Substantial
None

DOUGLAS BRIAN G BA-100S/N: BGD004

Accident Details

Date
Saturday, August 10, 2013
NTSB Number
CEN13LA478
Location
Killeen, TX
Event ID
20130812X25533
Coordinates
31.085832, -97.686386
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot’s improper management of the fuel mixture, which resulted in an over-rich fuel mixture condition and a subsequent partial loss of engine power.

Aircraft Information

Registration
N27BD
Make
DOUGLAS BRIAN G
Serial Number
BGD004
Year Built
2012
Model / ICAO
BA-100

Registered Owner (Historical)

Name
DOUGLAS BRIAN G
Address
448 CACTUS CIR
Status
Deregistered
City
KILLEEN
State / Zip Code
TX 76542-5025
Country
United States

Analysis

On August 10, 2013, about 0927 central daylight time, a Brian Douglas BA-100 airplane, N27BD, was substantially damaged during a forced landing near Killeen, Texas. The pilot, who was the sole occupant, was not injured. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed for the flight, which departed without a flight plan. The local flight originated from Skylark Field Airport (KILE), near Killeen, Texas, about 0925.

According to the pilot's statement, the airplane departed Runway 01 at KILE and the engine lost partial power while in the crosswind turn. The pilot considered turning back toward the runway, but elected not to because he was concerned that the airplane might enter into a spin. The pilot maneuvered the airplane and made a forced landing, during which both wings were structurally damaged during impact with trees.

Following the accident, the engine and fuel system were examined by an airframe and powerplant mechanic. Both fuel tanks were about ¾ full, with no evidence of fuel contamination. The magnetos and ignition leads were operable. Both spark plugs for the #1 cylinder were completely carbon fouled and the spark plugs for #2-#4 cylinders were significantly sooted. The pilot stated that he had set the engine mixture control to the full rich position during taxi and takeoff for the accident flight.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN13LA478