N98923

Substantial
None

CESSNA 172PS/N: 17276381

Accident Details

Date
Saturday, August 24, 2013
NTSB Number
ERA13CA377
Location
Mitchellville, MD
Event ID
20130826X54510
Coordinates
38.941112, -76.772224
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
4
Total Aboard
4

Probable Cause and Findings

The pilot’s decision to depart with a known deficiency following a hard landing. Contributing to the accident was an anomaly of the airplane’s nosewheel steering that could not be replicated during post-accident examination.

Aircraft Information

Registration
Make
CESSNA
Serial Number
17276381
Engine Type
Reciprocating
Year Built
1985
Model / ICAO
172PC172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
172P

Registered Owner (Current)

Name
COSTA FLYING SERVICE INC
Address
342 VICTORY HWY
City
PAINTED POST
State / Zip Code
NY 14870-9126
Country
United States

Analysis

The pilot reported that while taxiing for takeoff for a local flight with passengers, the right rudder felt “stiff.” Once in the air, the rudder operated normally; however, the pilot’s first landing was “hard.” After picking up a second set of passengers, the pilot noticed that while taxiing back to the runway, the right rudder felt even more stiff. At one point during the taxi, the pilot “stomped” on the rudder to steer the airplane right, but did not think much of the anomaly, as the airplane seemed to move normally after applying additional engine power. During the subsequent takeoff, the pilot noticed that the right rudder pedal continued to feel stiffer than it had during the previous takeoff.

During the second landing, the airplane veered immediately left upon touchdown and departed the runway. The pilot attempted to correct the airplane’s course, but the right rudder pedal was unresponsive. The pilot then attempted to abort the landing, but once in the air, he realized the airplane would not be able to climb above approaching trees and decided to land the airplane in a farm field. During the landing the nose landing gear collapsed and the airplane nosed over, resulting in substantial damage. A Federal Aviation Administration inspector examined the airframe and flight controls following the accident and confirmed that the rudder was free to move, but that the nose steering system of the airplane had been compromised during the accident and its pre-impact functionality could not be determined. When asked how the accident could have been prevented the pilot stated, “After a hard land[ing] have the plane inspected – Don’t takeoff even if it seems normal.”

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA13CA377