N9417Z

Substantial
None

CESSNA 172RS/N: 17280265

Accident Details

Date
Wednesday, March 5, 2014
NTSB Number
ERA14LA142
Location
Jackson, TN
Event ID
20140305X83714
Coordinates
35.599998, -88.915557
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A total loss of engine power due to maintenance personnel’s improper installation of the lower vacuum pump.

Aircraft Information

Registration
Make
CESSNA
Serial Number
17280265
Engine Type
Reciprocating
Year Built
1997
Model / ICAO
172RC72R
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
172R

Registered Owner (Current)

Name
AMERICAN AVIATION INC
Address
2495 BROAD ST
City
BROOKSVILLE
State / Zip Code
FL 34604-6841
Country
United States

Analysis

HISTORY OF FLIGHTOn March 5, 2014, about 1056 central standard time, a Cessna 172R, N9417Z, was substantially damaged during a forced landing after a loss of engine power during an instrument landing system (ILS) approach at McKellar Sipes Regional Airport (MKL), Jackson, Tennessee. The private pilot and his passenger were not injured. Instrument meteorological conditions prevailed, and an IFR flight plan had been filed for the flight destined for Augusta Regional Airport (AGS), Augusta, Georgia, conducted under Title14 Code of Federal Regulations Part 91.

According to the pilot, during the climb from MKL as he was at 6,500 feet above mean sea level (msl) he noted that he was losing oil pressure rapidly. He immediately did a 180 degree turn and headed on a direct course back to MKL.

A few miles from the airport, he asked for radar vectors for the "ILS RWY 2," and was vectored for the approach by air traffic control. Inbound on the ILS, he realized that he was too high, and executed a 360 degree descending turn to lose altitude. He then proceeded inbound on the ILS once again. At approximately 2,100 feet msl, the glideslope was "hopping from the top peg to the bottom peg rapidly" and he never was able to get a "solid indication from the glideslope." He continued to descend and when he was at approximately 1,500 feet msl, and still had not captured the glideslope, he executed a missed approach.

The pilot then climbed to 2,000 feet msl. There was now "zero oil pressure" and the engine would only produce partial power. He then circled around again and re-established himself on the localizer. He still had no glideslope indication and the glideslope needle was still "hopping from top to bottom." At this time the engine had lost all power and the airplane began descending. He was on the localizer and he knew he was lined up with the runway. At approximately 400 feet above the runway he still could not see the runway and the airplane was still descending with no engine power. The airplane continued to travel to the north of the airport and when the airplane was about 150 feet above ground level, the pilot saw a field and then a road. He then made a "sharp" left turn, lined up with the road and touched down. During the rollout, the right wing made contact with a highway sign, veered to the right and entered a cornfield. PERSONNEL INFORMATIONAccording to Federal Aviation Administration (FAA) and pilot records, the pilot held a private pilot certificate with ratings for airplane single-engine land, and instrument airplane. His most recent application for a FAA second-class medical certificate was dated August 20, 2009. The pilot reported that he had accrued approximately 275 total hours of flight experience, of which 215 hours were in the accident airplane make and model. AIRCRAFT INFORMATIONAccording to FAA and maintenance records the airplane was manufactured in 1997. The airplanes most recent annual inspection was completed on November 22, 2013. At the time of the inspection, the airplane had accrued 4036.1 total hours of operation.

METEOROLOGICAL INFORMATION

The recorded weather at MKL, included: wind 110 at 3 knots, 1/2 mile visibility in fog, variable visibility of 200 feet, temperature 0 degrees C, dew point -1 degrees C, and an altimeter setting of 30.21 inches of mercury. AIRPORT INFORMATIONAccording to FAA and maintenance records the airplane was manufactured in 1997. The airplanes most recent annual inspection was completed on November 22, 2013. At the time of the inspection, the airplane had accrued 4036.1 total hours of operation.

METEOROLOGICAL INFORMATION

The recorded weather at MKL, included: wind 110 at 3 knots, 1/2 mile visibility in fog, variable visibility of 200 feet, temperature 0 degrees C, dew point -1 degrees C, and an altimeter setting of 30.21 inches of mercury. WRECKAGE AND IMPACT INFORMATIONExamination of the accident site revealed that the road the pilot landed on was US Highway 70 and that after striking the highway sign it came to rest in a cornfield facing approximately 90 degrees from its direction of travel.

Examination of the wreckage by a Federal Aviation Administration inspector revealed that during the impact with the highway sign, and then the ground, the right wing incurred substantially damaged. Several large dents were visible, the lift strut was broken, the attach fittings and spar were damaged, and the wing tip was damaged.

Further examination revealed the presence of oil on the back of the engine, firewall, and belly. TESTS AND RESEARCHDuring the examination of the wreckage, it was revealed that the engine was still operable. The engine was started with the engine cowling removed and oil was observed to appear on the back of the accessory pad in the area of the lower vacuum pump. Further examination of the area revealed that the accessory drive adapter gasket was the source of the leak.

Review of maintenance records revealed that on March 4, 2014 (the day before the accident), at 4083.1 total hours of operation, the lower vacuum pump had been removed and a new vacuum pump had been installed along with a new shaft seal and accessory drive adapter gasket.

Review of invoice information and FAA Form 8130.3 Airworthiness Approval Tags indicated that the accessory drive adaptor gasket was part number 68315.

Examination of the gasket installed revealed that it was the proper gasket, however, it was discovered that it was distorted and showed signs of excessive compression and squeeze out.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA14LA142