N68828

Destroyed
Fatal

BOEING E75S/N: 75-5681

Accident Details

Date
Sunday, May 4, 2014
NTSB Number
WPR14FA182
Location
Fairfield, CA
Event ID
20140504X90153
Coordinates
38.264446, -121.924163
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot's failure to maintain clearance from the runway during a low-level aerobatic maneuver due to his impairment by an over-the-counter antihistamine. Contributing to the severity of the pilot's injuries were the pilot's lack of fire protective clothing, his inability to egress the cockpit, the rapid spread of the fire, and the decision of the air show's organizers not to have the airport rescue and firefighting services at their highest level of readiness, which delayed arrival of fire suppression equipment.

Aircraft Information

Registration
Make
BOEING
Serial Number
75-5681
Engine Type
Reciprocating
Year Built
1944
Model / ICAO
E75B752
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
E75

Registered Owner (Current)

Name
ANDREINI EDWARD
Address
2220 S CABRILLO HWY
City
HALF MOON BAY
State / Zip Code
CA 94019
Country
United States

Analysis

HISTORY OF FLIGHTOn May 4, 2014, about 1359 Pacific daylight time, a Boeing E75, N68828, was destroyed when it impacted runway 21R during an aerial demonstration flight at Travis Air Force Base (SUU), Fairfield, California. The commercial pilot/owner received fatal injuries. The exhibition flight was operated under the provisions of Title 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed, and no flight plan was filed for the flight.

The pilot was one of several civilian aerial demonstration pilots who performed at the 2-day SUU "Thunder Over Solano" open house, which included both static (ground) and aerial (flight) displays. According to United States Air Force (USAF) and Federal Aviation Administration (FAA) information, Friday, May 2, was the practice day, while the public event took place on Saturday and Sunday, May 3 and 4. The pilot flew two flight demonstration airplanes at the event; a North American P-51, and the accident airplane. All his flights preceding the accident flight were uneventful.

The accident occurred during a "ribbon-cut maneuver," whereby a ribbon was suspended transversely across the runway, between two poles held by ground crew personnel, and situated about 20 feet above the runway. The planned maneuver consisted of a total of three passes. The first two passes were to be conducted with the airplane upright, and were not planned to contact the ribbon. The final pass was to be conducted inverted, and the airplane would cut the ribbon with its vertical stabilizer. The first two passes were successful, but on the third (inverted, ribbon-cut) pass, the airplane was too high, and did not cut the ribbon. The pilot then initiated a fourth pass, and rolled the airplane inverted after aligning with the runway. The airplane contacted the runway prior to reaching the ribbon, slid inverted between the ground crew personnel holding the ribbon poles, and came to a stop a few hundred feet beyond them. A fire began as the airplane stopped. The pilot did not exit the airplane, and was fatally injured. PERSONNEL INFORMATIONThe 77-year-old pilot was a well known air show performer in the western United States. FAA records indicated that the pilot held a commercial pilot certificate, with single- and multi-engine airplane, and instrument airplane ratings, and was authorized to fly several experimental airplanes. His most recent FAA second-class medical certificate was issued in June 2013; on that application the pilot indicated that he had a total civilian flight experience of 11,400 hours. AIRCRAFT INFORMATIONFAA information indicated that the airplane was manufactured in 1944, and was first registered to the pilot in 1982. The airplane was equipped with a Pratt & Whitney R-985 series engine. The fuselage and empennage consisted of a synthetic-fabric covered steel tube structure, while the wings were primarily wood structure covered with the same type of fabric. The airplane was equipped with two tandem cockpits enclosed by a single canopy; the pilot flew the airplane from the aft cockpit.

The canopy consisted of a light metal frame (aluminum and steel) and plastic transparencies. The canopy was not part of the original airplane design or configuration. According to maintenance record information, and information provided by the pilot's family, the canopy was designed by the pilot with help from Serv Aero in Salinas, California. It was a modified version of the canopy from a "Varga" airplane, and had been installed on the accident airplane in November 1985. The canopy was intended to "improve air flow over the elevator and rudder for better flight control," and to provide additional cockpit comfort, in terms of reduced noise and wind blast.

The longitudinal section of the canopy consisted of one fixed panel (right side) and two movable panels (top and left side). The top panel was longitudinally hinged to the fixed right panel and the movable left panel, and the forward and aft bottom corners of the left panel rode in transverse tracks at the forward and aft ends of the cockpit. That design allowed cockpit entry and egress by operating the top and left canopy panels in a manner similar to a bi-fold door; which required approximately 18 inches of clearance above the canopy for the canopy to be opened.

The 47-gallon aluminum fuel tank was mounted in the center section of the upper wing, just forward of the cockpit. The main fuel tank was equipped with a central filler neck with a cap that protruded about 1.5 inches above the tank upper mold line. Four non-metallic flexible fuel lines, one near each lower corner of the main tank, enabled fuel to be supplied from the main tank.

An aluminum header fuel tank, of approximately 3 gallons capacity, was mounted in the fuselage forward of the cockpit. An oil tank for smoke generation was mounted below and slightly aft of the header tank. METEOROLOGICAL INFORMATIONThe SUU 1358 automated weather observation included wind from 240 degrees at 15 knots gusting to 21, visibility 10 miles, few clouds at 18,000 feet, temperature 22 degrees C, dew point 12 degrees C, and an altimeter setting of 29.99 inches of mercury. AIRPORT INFORMATIONFAA information indicated that the airplane was manufactured in 1944, and was first registered to the pilot in 1982. The airplane was equipped with a Pratt & Whitney R-985 series engine. The fuselage and empennage consisted of a synthetic-fabric covered steel tube structure, while the wings were primarily wood structure covered with the same type of fabric. The airplane was equipped with two tandem cockpits enclosed by a single canopy; the pilot flew the airplane from the aft cockpit.

The canopy consisted of a light metal frame (aluminum and steel) and plastic transparencies. The canopy was not part of the original airplane design or configuration. According to maintenance record information, and information provided by the pilot's family, the canopy was designed by the pilot with help from Serv Aero in Salinas, California. It was a modified version of the canopy from a "Varga" airplane, and had been installed on the accident airplane in November 1985. The canopy was intended to "improve air flow over the elevator and rudder for better flight control," and to provide additional cockpit comfort, in terms of reduced noise and wind blast.

The longitudinal section of the canopy consisted of one fixed panel (right side) and two movable panels (top and left side). The top panel was longitudinally hinged to the fixed right panel and the movable left panel, and the forward and aft bottom corners of the left panel rode in transverse tracks at the forward and aft ends of the cockpit. That design allowed cockpit entry and egress by operating the top and left canopy panels in a manner similar to a bi-fold door; which required approximately 18 inches of clearance above the canopy for the canopy to be opened.

The 47-gallon aluminum fuel tank was mounted in the center section of the upper wing, just forward of the cockpit. The main fuel tank was equipped with a central filler neck with a cap that protruded about 1.5 inches above the tank upper mold line. Four non-metallic flexible fuel lines, one near each lower corner of the main tank, enabled fuel to be supplied from the main tank.

An aluminum header fuel tank, of approximately 3 gallons capacity, was mounted in the fuselage forward of the cockpit. An oil tank for smoke generation was mounted below and slightly aft of the header tank. WRECKAGE AND IMPACT INFORMATIONThe airplane impacted runway 21R. Ground scars consisted of rudder/ vertical stabilizer ("tail") and upper wing contact (metal and wood scrapes, and paint transfer) with the runway, as well as propeller "slash marks" approximately perpendicular to the direction of travel. Review of image and ground scar data indicated that the airplane first contacted the runway with its right wing, followed by the tail, the left wing, and then the propeller.

The upper outboard right wing initial scar was followed about 7 feet later by the tail strike, and then a few feet later by the upper left wing. The initial tail strike was located about 45 feet right (northeast) of the runway centerline, about 380 feet beyond the runway threshold. The initial direction of travel was aligned approximately 5 degrees to the right (divergent from) the runway axis. The propeller slash marks began about 100 feet beyond the initial tail strike, and continued to the final resting location of the airplane. The slash marks described an arc, which curved to the left. The airplane slid inverted, and traveled a total distance of about 740 feet. It came to a stop near the left (southwest) edge of the runway, on a magnetic heading of about 140 degrees. Review of still and video imagery revealed that the airplane came to a stop about 13 seconds after it contacted the runway.

Examination of the wreckage indicated that most of the fabric covering on the fuselage was damaged or consumed by fire. The right wing and cockpit furnishings were almost completely consumed by fire, as were some of the aluminum flight control tubes. The left wing and rudder /vertical stabilizer sustained impact deformation, but the cockpit occupiable volume was not compromised by deformation of any surrounding structure.

The fuel lines and the main fuel tank were fire damaged, and at least two thermal penetrations of the main fuel tank were observed; both were consistent with an on-ground fire. The main tank fuel cap was found installed and latched. The cap/neck and surrounding tank skin appeared to be depressed slightly into the tank, but it could not be determined whether the cap and neck leaked fuel after the impact. No evidence of any provisions for increased crashworthiness of the fuel system, such as frangible, self-sealing line couplings, was observed in the wreckage. Due to the level of damage, the investigation was unable to determine the initial source(s) ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR14FA182