N97038

Substantial
Minor

CESSNA 182S/N: 18266947

Accident Details

Date
Saturday, May 24, 2014
NTSB Number
WPR14LA207
Location
Arvin, CA
Event ID
20140524X63615
Coordinates
35.201667, -118.833053
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot’s failure to reconnect the air-oil separator return line after completing an oil change, which resulted in a total loss of engine power due to oil starvation.

Aircraft Information

Registration
N97038
Make
CESSNA
Serial Number
18266947
Engine Type
Reciprocating
Model / ICAO
182C182
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SEIBOLD GUNTER W
Address
16741 MUSTANG DR
Status
Deregistered
City
SPRINGVILLE
State / Zip Code
CA 93265-9657
Country
United States

Analysis

On May 24, 2014, at 1211 Pacific daylight time, a Cessna 182Q, N97038, experienced a total loss of engine power and force landed in a field one mile south of Arvin, California. During the off airport landing the airplane nosed over, substantially damaging the tail and left lift strut. The airplane was registered to, and operated by, the commercial pilot under the provisions of 14 Code of Federal Regulations, Part 91, as a personal flight. Both the pilot and his single passenger received minor injuries. Visual meteorological conditions prevailed during the flight, and a visual flight plan was not filed. The flight originated at Corona Municipal Airport, Corona, California.The pilot stated that an hour into the flight, while over the Tehachapi Mountains, he noticed that the engine oil pressure had dropped, but the oil temperature and cylinder temperatures were normal. He declared an emergency to Bakersfield Approach and was initially given vectors to Bakersfield Municipal Airport. About 2-3 minutes later he started hearing rattling noises coming from the engine and then the cockpit filled with black smoke. He identified an open field on his left and maneuvered to make that field but didn't realize it had crop furrows. The airplane hit the first berm hard, bounced 3-4 times hitting berms along the way, then the nose wheel hit a berm and flipped the airplane over onto its back. On scene photos showed that the belly of the airplane was coated with engine oil aft of the engine fire wall.

An examination of the airplane and engine by the NTSB Investigator-in-Charge (IIC) and a technical representative from Continental Motors Incorporated was performed on September 30, 2014. The engine time indicated on the tachometer was 2,861.6 (hours). Investigators found the air-oil separator return line disconnected from the oil return port located on the rocker cover of the engine's number 1 cylinder. Oil staining was evident on the lower engine cowling below the number 1 cylinder. It was noted that the engine oil filter was located behind the air-oil separator return line. The left engine case half, upper section above the No 4 cylinder, exhibited a 6 x 4 inch hole just aft of the oil filler neck. The cylinders were removed and the case was separated into its halves. The crankshaft main bearings exhibited normal wear with no heat discoloration. The number 3 crankshaft throw bearing was shiny & polished showing very little heat discoloration. The number 4 crankshaft throw was dark black with a few gouges and exhibited extreme heat distress. The number 5 crankshaft throw was black and exhibited extreme heat distress. The number 6 connecting rod attached to the crankshaft throw was discolored dark gray, consistent with heat distress. The internal section of the engine case in line with the number 3 & 4 crankshaft throws exhibited internal repeated impact marks, metal removal, and damage to the oil galleries on both sides of the engine case.

Examination of the engine logbook revealed that the most recent annual inspection was performed on April 10, 2013, 2,828.2 hours total time, and 309.5 hours since major overhaul (SMOH). The last entry in the logbook was dated April 18, 2014, where the pilot/owner had performed an oil change, 2,857.3 hours total time

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR14LA207