N206ND

Substantial
None

DIAMOND AIRCRAFT IND INC DA20-C1S/N: C0020

Accident Details

Date
Sunday, June 1, 2014
NTSB Number
CEN14LA267
Location
Longmont, CO
Event ID
20140601X00617
Coordinates
40.169090, -105.209907
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A loss of engine power due to fuel exhaustion. Contributing to the accident was the pilot’s inadequate preflight inspection.

Aircraft Information

Registration
N206ND
Make
DIAMOND AIRCRAFT IND INC
Serial Number
C0020
Engine Type
Reciprocating
Year Built
1998
Model / ICAO
DA20-C1DV20
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
KOSAIR INC
Address
12826 WATERBURY RD
Status
Deregistered
City
LONGMONT
State / Zip Code
CO 80504-1163
Country
United States

Analysis

On June 1, 2014, about 0915 mountain daylight time, a Diamond DA 20-C1, N206ND, collided with terrain after the engine lost power near Longmont, Colorado. The commercial pilot, the sole occupant on board, was not injured. The airplane was substantially damaged. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed at the time of the accident, and no flight plan had been filed. The local flight was originating when the accident occurred.

In a telephone interview, the pilot said the airplane had just come out of an annual inspection and his mechanic had performed a post-maintenance engine functional test up to full power. All systems operated normally and the engine performed well. The accident flight was a test flight after the annual inspection. The pilot said prior to takeoff, he also ran the engine up to full power. No anomalies were noted. The pilot took off and after climbing to about 400 feet, the engine lost power. The pilot made a forced landing in a field adjacent to the airport. The airplane struck the ground nose first, shearing off the nose gear, and skidded about 150 feet before coming to a stop. The empennage was separated from the fuselage.

On June 4, three Federal Aviation Administration inspectors examined the airplane in the presence of the pilot. According to the lead inspector, the airplane was equipped with two fuel drains --- one for the fuel tank and one for the gascolator. Only a few drops of fuel were recovered from each drain. No fuel could be seen in the fuel tank. The pilot said fuel had been leaking from the fuel tank for three days before the FAA inspectors arrived. According to the FAA inspector's report, if there had been minimal fuel aboard the airplane, fuel greater than a few drops would have drained out of the gascolator drain during the examination.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN14LA267