N508CT

Substantial
Fatal

FLIGHT DESIGN GMBH CT-SW 2006S/N: 06-10-06

Accident Details

Date
Saturday, July 5, 2014
NTSB Number
ERA14LA329
Location
Gasport, NY
Event ID
20140707X41002
Coordinates
43.181110, -78.556945
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot's failure to maintain adequate airspeed following a left turn during takeoff, which led to the airplane exceeding its critical angle-of-attack and experiencing an aerodynamic stall.

Aircraft Information

Registration
N508CT
Make
FLIGHT DESIGN GMBH
Serial Number
06-10-06
Engine Type
Reciprocating
Year Built
2006
Model / ICAO
CT-SW 2006FDCT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SCHNABEL JOHN A
Address
118 COUNTRYSIDE LN
Status
Deregistered
City
WILLIAMSVILLE
State / Zip Code
NY 14221-1308
Country
United States

Analysis

HISTORY OF FLIGHT

On July 5, 2014, about 1104 eastern daylight time, a Flight Design GMBH CT-SW 2006, N508CT, collided with trees then the ground shortly after takeoff from Royalton Airport, Gasport, New York. The private rated pilot, the sole occupant was fatally injured, and the airplane was substantially damaged. The airplane was registered to and operated by a private individual under the provisions of 14 Code of Federal Regulations (CFR) Part 91 as a personal, local flight. Visual meteorological conditions prevailed at the time and no flight plan was filed. The flight was originating at the time of the occurrence.

According to Federal Aviation Administration (FAA) personnel, witnesses reported the pilot performed an engine run-up at the approach end of runway 7, then back taxied down the runway where he turned around and initiated takeoff from runway 25. At rotation the airplane appeared to pitch up higher than normal followed by up and down pitch oscillations and left bank oscillations, climbing no higher than approximately 75 feet. The airplane also began a slow bank to the left, before impacting trees south of the runway in a left wing low attitude. The airplane came to rest nearly inverted on an easterly heading in a heavily wooded area. Witnesses called 911 to report the accident and the pilot was rescued and transported to a hospital, where he died on July 16, 2014.

PERSONNEL INFORMATION

The pilot, age 78, held an airline transport pilot certificate with rating(s) airplane multi-engine land; at the airline transport pilot level he held type ratings in B727 and DC-9. He held a commercial pilot certificate with rotorcraft helicopter, and instrument helicopter ratings; at the commercial level he was type rated in a SK-58. He also held a private pilot certificate with airplane single engine land rating, and held flight engineer certificate with turbojet and turboprop ratings. He held a third class medical certificate with a limitation to have available glasses for near vision on May 24, 2011. On the application for the last medical certificate he listed a total time of 30,225 hours, and his weight was listed as 222 pounds. There were no records of previous accidents or incidents or FAA enforcement actions.

A review of the pilot's pilot logbook from September 12, 2012, to the last entry dated May 21, 2014, revealed he logged 20 flights in the airplane totaling 34.5 hours. The first flight of September 17, 2012, was associated with the date he purchased the airplane and was logged as dual received and also as pilot-in-command (PIC). The remainder of the flights were only logged as PIC.

AIRCRAFT INFORMATION

The airplane was manufactured in 2006 by Flight Design GmbH, as model CT-SW 2006, and was designated serial number 06-10-06. It was powered by a Rotax 912 ULS carbureted engine rated for 5 minutes maximum at 100 horsepower at 5,800 rpm, or 95 horsepower maximum continuous performance at 5,500 rpm. It was equipped with a fixed pitch propeller.

Review of the maintenance records revealed the airplane was last inspected in accordance with an annual inspection that was signed off on June 24, 2014. The airframe logbook entry indicated in part that the autopilot computer was overhauled at the factory, and an invoice provided by the pilot's son indicated the inoperative roll servo was removed and a loaner roll servo was installed and rigged. The airplane total time at that time was reported to be 317.1 hours. Excerpts from the airframe maintenance records are contained in the NTSB public docket.

According to the mechanic who performed the last annual inspection, following installation of the overhauled autopilot computer and loaner roll servo, he test flew the airplane twice totaling about 1.2 hours. During both flights he operated the autopilot later reporting no discrepancies with the system including the loaner roll servo.

METEOROLOGICAL INFORMATION

A surface observation weather report taken at Buffalo Niagara International Airport (BUF), Buffalo, New York, at 1054, or approximately 10 minutes before the accident indicates the wind was from 260 degrees at 8 knots, the visibility was 10 statute miles, and few clouds existed at 25,000 feet. The temperature and dew point were 22 and 09 degrees Celsius respectively, and the altimeter setting was 30.25 inches of Mercury (inHg). The accident site was located about 16 nautical miles and 28 degrees from BUF.

AIRPORT INFORMATION

The Royalton Airport is a public-use airplane equipped with a single runway designated 7/25; the airport elevation is 628 feet. The asphalt runway is 2,530 feet long and 35 feet wide.

FLIGHT RECORDERS

The airplane was equipped with a Rotax Flydat engine recording device that recorded and retained engine data associated with time, exhaust gas temperature, pressure, engine rpm, water temperature and oil temperature. The airplane was also equipped with a Garmin 396 GPS. Both devices were removed from the airplane and sent to the NTSB Vehicle Recorder Laboratory located in Washington, D.C. The Flydat was subsequently hand carried by a NTSB investigator to Rotax's facility in British Columbia, for readout. The data was provided to a NTSB specialist in Washington, D.C. The GPS was read-out by the NTSB specialist located in Washington, DC.

According to the NTSB specialist's factual report, correlation of the data recorded by the FLYdat and the GPS data was performed which resulted in an error of plus or minus 3 seconds. Based on the GPS data, the groundspeed began to increase between 1104:02, and 1104:10. The airplane accelerated to 32 knots groundspeed while maintaining runway heading at 1104:19. The next data point 1 second later, while over the runway, indicates the airplane had accelerated to 39 knots groundspeed, the altitude was 6 feet higher, and the heading had changed over 5 degrees to the left. Five seconds later, or at 1104:25, the airplane was over trees south of the runway, had attained the maximum recorded groundspeed value of 41 knots, the altitude was recorded to be 679 feet, and the heading was recorded to be 207.5 degrees.

Plotting on a map of GPS data and correlation of the FLYdat and GPS data revealed that during the takeoff while over the runway, the engine rpm increased to 3,230 rpm, and remained at that value for about 5 seconds. The rpm dropped about 50 rpm, then increased to the maximum recorded value of 4,590 rpm at 1104:32, which was the last FLYdat data point. The last valid in-flight data point from the GPS was determined to be at 1104:25.

Review of FLYdat data for the previous flight revealed that during takeoff, the engine rpm sharply increased to about 5,000, and remained at the value until being reduced. A report from the NTSB specialist regarding the FLYdat and GPS, and the data downloaded from the FLYdat and GPS are contained in the NTSB public docket.

WRECKAGE AND IMPACT INFORMATION

The airplane crashed in a heavily wooded area south of the runway and came to rest nearly inverted on a nearly due east heading at 43 degrees 10.87 minutes North latitude and 078 degrees 33.41 minutes West longitude. That location when plotted was located about 180 feet south of the southern edge of the runway, and 242 feet and 133 degrees from the last GPS in-flight target.

Following recovery of the airplane, it was inspected by representatives of the FAA along with a representative of the airframe manufacturer. The examination determined that the flaps were symmetrically extended 15 degrees, which equated to the flap selector. The ballistic parachute was not deployed, and inspection of the flight controls for roll, pitch, and yaw revealed no evidence of preimpact failure or malfunction.

Examination of the cockpit revealed the choke was off, the throttle was full forward, and the brake was off. The ballistic parachute activation safety pin remained in place in the activation handle. The airspeed indicator was near 0. The on-board FLYdat engine monitor and Garmin 396 GPS receiver were retained and sent to the NTSB Vehicle Recorder Division for read-out.

Following recovery of the airplane, examination of the engine was performed by a representative of the engine manufacturer with FAA oversight. The inspection revealed crankshaft, camshaft and valve train continuity was confirmed; compression was noted in all cylinders. During hand rotation of the engine, no unusual sounds were noted coming from the gearbox. Impact damage was noted to the radiator, but coolant was noted in the expansion tank. The carburetor bowls were removed and corrosion was noted inside. The engine was shipped to a facility for an attempted engine run.

Operational testing of the engine was performed with FAA oversight; a calibrated test club propeller pitched for 5,600 rpm was installed. In preparation for the engine run, the oil tank was replaced in order to avoid possible contamination and the muffler was replaced because it was crushed. The engine was placed on a test stand with no additional work performed, and the oil system was then purged of air in advance of the attempted engine run. While priming the fuel system, a slight fuel leak was noted in a location between the fuel pump and carburetor. The engine was started and operated to 5,600 rpm remaining at that setting for about 2 minutes. The magnetos checked good and the engine was operated using the ignition system components installed at the time of the accident. During the engine run the oil pressure and oil temperature were within limits and no discrepancies were noted. The engine was secured, and then operated a 2nd time with no discrepancies noted. A copy of the report from the engine manufacturer representative is contained in the NTSB public docket.

Examination of the three bladed propeller revealed all blades were fractured at varying lengths.

MEDICAL AND PATHOLOGICAL INFORMATION

The pilot was reported by his son to be in good health on the day of the accident; the pilot di...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA14LA329