N13SK

Substantial
None

CESSNA 172NS/N: 17271183

Accident Details

Date
Wednesday, July 16, 2014
NTSB Number
CEN14LA374
Location
Rockville, IN
Event ID
20140717X83755
Coordinates
39.761245, -87.226934
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A partial loss of engine power due to a failure of the dual magneto system. Contributing to the accident was the improper maintenance of the duel magneto system.

Aircraft Information

Registration
Make
CESSNA
Serial Number
17271183
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
172NC172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
172N

Registered Owner (Current)

Name
FLYDREAMS AIRCRAFT GROUP INC
Address
1801 S PERIMETER RD STE 180
City
FORT LAUDERDALE
State / Zip Code
FL 33309-7140
Country
United States

Analysis

On July 16, 2014, about 1450 eastern daylight time, a Cessna 172N airplane, N13SK, was substantially damaged during a forced landing near Rockville, Indiana. The pilot and passenger were not injured. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Day visual meteorological conditions prevailed for the flight, which operated without a flight plan. The local flight departed from a private airport near Rockville, Indiana about 1400.

According to the pilot, the engine lost partial power while in cruise flight. The pilot attempted to restore engine power by applying carburetor heat and checking the mixture and fuel selector positions, but engine performance continued to worsen. The pilot performed a forced landing into a corn field, during which both wings were damaged.

During examination of the engine, both points of the single drive/dual magneto system would not open; as the center cam was rotated to the 'points open' position, both points remained closed. Further examination revealed that four screws designed to hold the magneto points in their operational position had become loose. Two of the loose screws did not have any torque paint on them; torque paint for the other two loose screws was missing from the screw slot.

Aircraft records indicted the airplane had flown eight hours since its last annual inspection on February 3, 2014. The investigation was not able to interview the mechanic who performed this annual inspection and recent maintenance on the airplane.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN14LA374