N6743Q

Substantial
None

GRUMMAN ACFT ENG COR-SCHWEIZER G 164AS/N: 1715

Accident Details

Date
Friday, July 18, 2014
NTSB Number
CEN14LA375
Location
Fairview, KS
Event ID
20140718X25106
Coordinates
39.853889, -95.729721
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The backfire of the engine and its loss of power for reasons that could not be determined based on the available evidence.

Aircraft Information

Registration
N6743Q
Make
GRUMMAN ACFT ENG COR-SCHWEIZER
Serial Number
1715
Engine Type
Turbo-shaft
Model / ICAO
G 164AG64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
2155 VERMONT RD
Status
Deregistered
City
RANTOUL
State / Zip Code
KS 66079-9014
Country
United States

Analysis

On July 18, 2014, about 0845 central daylight time, a Grumman G-164A airplane, N6743Q, made a forced landing on a road following a loss of engine power near Fairview, Kansas. The pilot, who was the sole occupant, was not injured. The airplane sustained substantial damage. The airplane was registered to and operated by Precision Aerial Ag LLC, under the provisions of 14 Code of Federal Regulations Part 91 as a positioning flight. Visual meteorological conditions prevailed and no flight plan was filed. The flight departed the Amelia Earhart Airport (K59), Atchison, Kansas, at 0830 and was en route to the Sabetha Municipal Airport (K83), Sabetha, Kansas.

According to the pilot's statement, he was ferrying the airplane and was cruising at 600 feet above ground level. The airplane's engine began to "backfire very loudly" and experienced a partial loss of power. He descended and lined up to land on a rural road; he noticed a car on the road so he circled over a field and attempted to landing on the road again. During the landing, the engine experienced a total loss of power and the airplane stalled, which resulted in a bounced hard landing.

According to the responding Federal Aviation Administration (FAA) inspector, after landing the airplane slid sideways into a telephone pole which resulted in damage to the wings and fuselage. One of the two propeller blades had a slight bend. Due to impact damage the engine was not able to be test run. The engine continuity was confirmed as the crankshaft rotated without obstruction. The fuel tanks contained fuel. The magnetos both rotated freely and produced a spark. The induction air filter was protruding outward and opposite from the direction of normal airflow. One of the rocker box covers sustained impact damage. No other anomalies were noted on scene.

The airplane was recovered to a storage facility for examination by the FAA inspector and an engine mechanic. On August 1, 2014, the inspector witnessed the removal of the No. 2 cylinder. The oil control ring in the cylinder was broken. The intake valve operated with no anomalies noted and did not display any damage. The induction air filter bracket and frame were distorted and the filter could not be removed. No other anomalies were noted with the engine.

A review of the engine maintenance logbooks revealed that a major engine overhaul was completed on November 12, 1996. On February 4, 2014 an annual inspection was completed and determined to be in airworthy condition. On July 17, 2014 the No. 5 pushrod tube was resealed.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN14LA375