N6629V

Substantial
Fatal

BELLANCA 17-30AS/N: 30312

Accident Details

Date
Sunday, November 30, 2014
NTSB Number
CEN15FA060
Location
Boonville, MO
Event ID
20141130X22258
Coordinates
38.935276, -92.684165
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
1
Serious Injuries
3
Minor Injuries
0
Uninjured
0
Total Aboard
4

Probable Cause and Findings

The pilot's failure to maintain adequate airspeed during a forced landing following a total loss of engine power due to fuel starvation, which resulted in the airplane exceeding its critical angle of attack, and an aerodynamic stall at a low altitude. Contributing to the accident was the pilot’s improper fuel management.

Aircraft Information

Registration
N6629V
Make
BELLANCA
Serial Number
30312
Year Built
1970
Model / ICAO
17-30A

Registered Owner (Historical)

Name
SALE REPORTED
Address
128 S 11TH ST
Status
Deregistered
City
SALINA
State / Zip Code
KS 67401-2569
Country
United States

Analysis

HISTORY OF FLIGHTOn November 30, 2014, about 0857 central standard time (CST), a Bellanca model 17-30A single-engine airplane, N6629V, was substantially damaged when it collided with terrain during landing approach to runway 36 at Jesse Viertel Memorial Airport (VER), Boonville, Missouri. The commercial pilot was fatally injured and his three passengers were seriously injured. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 without a flight plan. Day marginal visual meteorological conditions prevailed for the cross-country flight that departed Spirit of St. Louis Airport (SUS), Chesterfield, Missouri, about 0740, and was originally destined for Charles B. Wheeler Downtown Airport (MKC), Kansas City, Missouri.

The day preceding the accident, the pilot had flown from MKC to SUS. After landing, about 1207, the pilot told a fixed-base operator (FBO) line technician that he had a depleted battery because of an unspecified charging system malfunction. The pilot, who also was an aviation mechanic, removed the battery from the airplane to have it charged. About 1800, the pilot returned to the FBO with the recharged battery. After reinstalling the battery, the pilot started and ran the engine for about 5 to 7 minutes. Following the engine run, the pilot removed the cowling and began adjusting a subcomponent of the alternator control unit (ACU). After adjusting the ACU, the pilot performed another engine test run that lasted about 10 minutes. Following the second engine test run, the pilot told the FBO line technician that the airplane's ammeter was still showing a slight discharge while the engine was running, and that he was uncomfortable departing at night with a charging system issue. The pilot asked if he and his passengers could stay the night in the pilot's lounge so they could depart early the following morning. The pilot also asked for the airplane to be towed to the self-serve fuel pumps because he did not want to deplete the battery further with another engine start.

The pilot prepaid for 20 gallons of fuel at the self-serve fuel pump. According to the line technician, the pilot nearly topped-off the right inboard fuel tank with 13 gallons before switching over to the left inboard tank. Upon a visual inspection of the left inboard tank, the pilot told the line technician that it contained less fuel than he had expected. The pilot proceeded to add the remaining 7 gallons of the prepaid 20 gallons to the left inboard fuel tank. The line technician noted that after fueling the left inboard fuel tank, the fluid level was about 2 inches from the top of the tank. The pilot did not purchase any additional fuel and told the line technician that both outboard "auxiliary" fuel tanks were nearly full. The line technician then towed the airplane back to the ramp for the evening. The line technician reported that the airplane departed FBO ramp the following morning.

According to air traffic control (ATC) data, the first radar return for the accident flight was shortly after the airplane departed from runway 26L at 0740:50 (hhmm:ss). The airplane initially transmitted a visual flight rules (VFR) beacon code (1200) during accident flight. The plotted radar track revealed the airplane flew west-northwest from SUS toward the planned destination. At 0751:03, the airplane stopped transmitting a 1200 beacon code and continued as a primary-only radar target. The location of the final 1200 code was about 21.5 miles west-northwest of SUS at 2,400 ft mean sea level (msl). The lack of a reinforced beacon return was consistent with the pilot turning the airplane transponder off. The primary-only radar track continued west-northwest at an unknown altitude. (The airplane's transponder transmits altitude data to the radar facility; a primary-only radar return does not include altitude data) At 0832:04, the airplane was still traveling west-northwest and was about 5 miles south of Jesse Viertel Memorial Airport (VER). At 0836:21, the airplane descended below available radar coverage about 11 miles west-southwest of VER. There was no radar coverage with the airplane for about 19 minutes. At 0855:30, the radar facility began tracking a VFR reinforced beacon return (1200) about 2.3 miles north of VER descending through 1,500 feet msl. The time and location of the radar returns are consistent with the accident flight maneuvering to land at VER. The airplane entered a left downwind for runway 36 at 1,200 feet msl. At 0856:49, the last recorded radar return was about 0.9 mile southwest of the runway 36 threshold at 1,100 feet msl (about 400 feet above the ground).

According to one of the surviving passengers, while enroute at an altitude of 2,000 to 3,000 ft msl, the airplane encountered a line of "dense clouds" near Sedalia, Missouri. The pilot attempted to navigate beneath the clouds, at an altitude of about 1,500 ft msl, before deciding to make a course reversal and divert to a nearby airport. The pilot told the passenger, who was seated in the forward-right seat, to be on the lookout for towers and obstructions because of their low proximity to the ground. The passenger reported that after flying east for a few minutes the pilot identified VER on his Apple iPad Mini. The flight approached the airport traffic pattern from the west and made a left base-to-final turn toward runway 36. The passenger reported that the landing gear extended normally. However, when the pilot reduced engine power, in attempt to reduce airspeed, the engine experienced a loss of power. The pilot was able to restore engine power briefly by advancing the throttle, but the engine quickly lost total power. The passenger reported that the pilot then began making rapid changes to the engine throttle and mixture control without any noticeable effect to engine operation. The passenger stated that as the pilot prepared for a forced landing the airplane encountered an aerodynamic stall about 250 ft above the ground. The passenger did not recall the airplane impacting the ground. PERSONNEL INFORMATIONAccording to Federal Aviation Administration (FAA) records, the 63-year-old pilot held a commercial pilot certificate with single engine land, single engine sea, multiengine land, and instrument airplane ratings. He also held a flight instructor certificate with single engine, multiengine, and instrument airplane ratings. The pilot's last aviation medical examination was on April 11, 2014, when he was issued a third-class medical certificate with a limitation for corrective lenses. A search of FAA records showed no previous accidents, incidents, or enforcement proceedings. The pilot completed a flight review, as required by FAA regulation 61.56, on November 12, 2014, in a single-engine Cessna model 180 airplane.

The pilot's flight history was reconstructed using his pilot logbook and a computer spreadsheet. The last flight entry in the pilot logbook was dated January 8, 2012. The computer spreadsheet was last updated on November 16, 2014, at which time he had accumulated 3,036 hours total flight time, of which 2,955 hours were listed as pilot-in-command. He had accumulated 2,428 hours in single engine airplanes and 608 hours in multi-engine airplanes. Additionally, he had logged 43 hours in actual instrument meteorological conditions, 175 hours in simulated instrument meteorological conditions, and 233 hours at night.

According to available logbook documentation, the pilot had flown 19 hours during the previous 6 months, 10 hours during prior 90 days, and 3 hours in the month before the accident flight. According to a flight-monitoring website, FlightAware.com, the pilot had flown 1.3 hours during the 24-hour period preceding the accident flight. AIRCRAFT INFORMATIONThe accident airplane was a 1970 Bellanca model 17-30A, Super Viking, serial number 30312. The Super Viking is a single-engine, low wing monoplane with an all-wood wing construction and a fabric covered steel-tube fuselage. A 300-horsepower Continental Motors model IO-520-K reciprocating engine, serial number 209048-70K, powered the airplane through a constant speed, three blade, Hartzell model HC-C3YF-1RF propeller. The airplane had a retractable tricycle landing gear, was capable of seating the pilot and three passengers, and had a maximum gross weight of 3,325 pounds. The FAA issued the accident airplane a standard airworthiness certificate on October 23, 1970. The pilot purchased the airplane on July 5, 2014.

The airplane's recording tachometer meter indicated 621.4 hours at the accident site. The airframe and engine had accumulated a total service time of 2,858.7 hours. The engine had accumulated 1,429.7 hours since the last major overhaul completed on December 10, 1976. The engine had accumulated 206.1 hours since a top overhaul that was completed on December 8, 2007. The last annual inspection of the airplane was completed on November 1, 2014, at 2,853.5 total airframe hours. The airplane had accumulated 5.2 hours since the last annual inspection. A postaccident review of the maintenance records found no history of unresolved airworthiness issues. METEOROLOGICAL INFORMATIONThe National Weather Service (NWS) Surface Analysis Chart for 0900 CST depicted a strong cold front immediately east of the accident site. The front stretched across Missouri between the departure airport and the planned destination. The cold front was associated with a defined wind shift and low stratiform clouds behind the front. There were several weather stations located near the accident site that had surface visibility restrictions in fog and mist. Weather radar imagery did not depict any significant weather echoes in the area of the accident site; however, the weather radar did detect a fine line of very light intensity echoes associated with the cold front. Satellite imagery depicted a band of low stratiform clouds extending over the accident site westward ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN15FA060