N32396

Substantial
Fatal

PIPER PA-28-140S/N: 28-7525060

Accident Details

Date
Sunday, March 29, 2015
NTSB Number
ERA15FA170
Location
Orange, VA
Event ID
20150329X15652
Coordinates
38.251388, -78.037223
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The student pilot's failure to maintain adequate airspeed after takeoff, which resulted in the airplane exceeding its critical angle-of-attack and experiencing an aerodynamic stall.

Aircraft Information

Registration
N32396
Make
PIPER
Serial Number
28-7525060
Engine Type
Reciprocating
Year Built
1974
Model / ICAO
PA-28-140P28A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
GRACE FLIGHT LLC
Address
19103 CONSTITUTION HWY
Status
Deregistered
City
ORANGE
State / Zip Code
VA 22960-4414
Country
United States

Analysis

HISTORY OF FLIGHTOn March 29, 2015, about 0940 eastern daylight time, a Piper PA-28-140, N32396, impacted terrain during takeoff from Orange County Airport (OMH), Orange, Virginia. The airplane was substantially damaged, and the student pilot was fatally injured. Visual meteorological conditions prevailed and no flight plan was filed for the flight, which was operated by Skyline Aviation Services. The solo instructional flight was destined for Farmville Regional Airport (FVX), Farmville, Virginia, and was conducted under the provisions of Title 14 Code of Federal Regulations Part 91.

The owner of the flight school was also a flight instructor (CFI) who had flown with the student on several occasions. She stated that the student was departing on his first solo cross-country flight when the accident occurred. The morning of the accident, she reviewed his preflight planning, endorsed his logbook for the flight, and assisted him in a preflight inspection of the airplane and engine run-up check. She stated that she observed no anomalies with the airplane. The pilot then taxied the airplane to the other side of the airport to obtain fuel, then performed a second engine run-up and departed from runway 08. She stated that the takeoff appeared normal, but the pilot initiated a left turn to the crosswind leg of the traffic pattern earlier than was customary. As the airplane turned left, its nose pitched up abruptly, and it rolled sharply left and descended to ground contact. The CFI immediately called 911 and responded to the accident site to render assistance.

Two pilot-rated witnesses located on the north side of the airport observed the airplane during the takeoff and provided written statements to local law enforcement. They remarked to each other that the airplane appeared "abnormally slow" and stated that it did not seem to be gaining altitude. Both individuals also reported viewing a thin trail of "smoke" or "brown exhaust" from the airplane's engine. The witnesses observed the airplane make a sharp left turn from an altitude about 150 feet above ground level, and descend steeply to ground contact. One of the witnesses reported that the wind at the time of the accident was light and variable from the north and east. In subsequent, separate telephone interviews, both witnesses stated that they did not observe any birds in the vicinity of the airport at the time of the accident. Additionally, neither of the witnesses perceived any changes or abnormalities in the airplane's engine noise during the takeoff, though one of the witnesses reported that the engine sounded "quieter than it should be."

Another witness reported that he was driving parallel to the runway at OMH. He reported seeing the accident airplane accelerate down the runway, and stated that it "looked like it was having trouble" shortly after it became airborne. He observed the airplane's nose pitch up twice, and also observed a trail of black smoke that extended the length of the airplane. He stated that the airplane appeared to "level out," then made a "hard" left turn as the nose dropped. The airplane then disappeared from his view behind trees and terrain. PERSONNEL INFORMATIONThe pilot held a student pilot certificate and Federal Aviation Administration (FAA) third-class medical certificate, which was issued on January 20, 2015. Review of the pilot's logbook revealed that he had accumulated 30.6 total hours of flight experience, of which about 18 hours were in the accident airplane, and 2.7 hours were solo. AIRCRAFT INFORMATIONThe airplane was manufactured in 1974, and was originally equipped with a Lycoming O-320 series, 150 hp reciprocating engine. In 2002, the engine was overhauled and equipped with a Penn Yan Aero RAM160 supplemental type certificate, which resulted in an increase to 160 hp. Review of maintenance logs indicated that the airplane's most recent 100-hour inspection was completed on February 20, 2015, at a total airframe time of 5,156 hours. At the time of the accident, the airplane had accrued 5,187.6 hours in operation.

According to the owner of the flight school, the school had operated the accident airplane under a lease agreement for about 18 months prior to the accident, and had purchased the airplane about 3 weeks prior to the accident. METEOROLOGICAL INFORMATIONThe 0935 weather observation at OMH included wind from 040 degrees at 3 knots, 10 miles visibility, clear skies, temperature 0 degrees C, dew point -12 degrees C, and an altimeter setting of 30.41 inches of mercury. AIRPORT INFORMATIONThe airplane was manufactured in 1974, and was originally equipped with a Lycoming O-320 series, 150 hp reciprocating engine. In 2002, the engine was overhauled and equipped with a Penn Yan Aero RAM160 supplemental type certificate, which resulted in an increase to 160 hp. Review of maintenance logs indicated that the airplane's most recent 100-hour inspection was completed on February 20, 2015, at a total airframe time of 5,156 hours. At the time of the accident, the airplane had accrued 5,187.6 hours in operation.

According to the owner of the flight school, the school had operated the accident airplane under a lease agreement for about 18 months prior to the accident, and had purchased the airplane about 3 weeks prior to the accident. WRECKAGE AND IMPACT INFORMATIONThe airplane came to rest upright in a field located about 1,330 feet northeast of the departure end of runway 08, with the wreckage oriented on a heading of about 170 degrees magnetic. The initial impact point was identified by a ground scar about 30 feet south of the main wreckage that contained pieces of the left wing navigation light. Areas of disturbed soil extended north from the initial impact point about 15 feet toward a large impact crater about 6 feet in length and 3 feet in width, which contained pieces of the propeller spinner and ground scars consistent with propeller contact.

The propeller remained attached to the crankshaft flange and one blade exhibited slight forward bending. Both blades displayed chordwise scratching and leading edge gouging. The engine remained attached to the fuselage by its bottom mounts. The fuselage displayed significant aft crushing from the engine firewall to the rear cabin seats, and was displaced to the left just aft of the baggage area.

Both left and right wings displayed significant aft crushing of their leading edges. The left wing was separated from the fuselage at its root and the fuel tank was breached. Residual fuel was found inside, and the fuel tank cap was in place and secure. The left aileron remained attached at its hinge points. Control continuity was established from the aileron to the cockpit area through cable breaks at the wing root that displayed signatures consistent with overstress failure.

The right wing remained attached to the fuselage at its root. The outboard approximate 4 feet was bent upward about 45 degrees. The right fuel tank was breached and leaking fuel; the right fuel tank cap was in place and secure. The right aileron remained attached at its hinge points and control continuity was established from the aileron to the cockpit area. The wing flaps were fully retracted.

The empennage was intact and displayed minor impact damage. The rudder remained attached to the vertical stabilizer at its hinge points, and the stabilator remained attached at its mounting blocks. Rudder and stabilator control continuity was established to the cockpit area. The stabilator trim screw indicated a trim position between neutral and full nose-up trim. The windscreen and left cabin window were destroyed upon impact, and pieces of each were distributed along the wreckage path and around the main wreckage. Examination of the wings, empennage, and windscreen pieces did not reveal any evidence of a bird strike.

The carburetor heat control was in the "off" position, and the engine primer was in and locked. The fuel selector was in the right tank position, and could not be manipulated due to impact damage.

The engine crankshaft was rotated by hand at the propeller hub and continuity of the valve and powertrains was confirmed. The spark plugs were removed and displayed black carbon fouling. The #1 and #3 cylinder bottom plugs were oil-covered; consistent with the engine's postimpact orientation. Thumb compression was obtained on all cylinders, and borescope examination of the cylinders revealed no anomalies. The carburetor inlet screen was absent of debris. The carburetor was removed and the bowl was opened. The floats were intact, and the bowl contained fuel consistent with the color and odor of 100 low lead aviation fuel and was absent of contamination. The magnetos remained secured to their mounts, and were removed and actuated by hand. Each magneto produced spark at all of its terminal leads.

The airplane was examined at a secure storage facility on April 29, 2015. The pilot's seat was secure on the track, and the seat position adjustment lever functioned properly when manipulated. Neither the seat track nor the locking pins displayed any abnormal or excessive wear. The spark plugs were tested for operation. Three of the eight plugs produced weak and intermittent spark. One plug produced no spark; however, this plug was likely damaged during postaccident removal from the engine.

The stall warning switch was removed for testing and electrical continuity was confirmed when the switch was manipulated. ADDITIONAL INFORMATIONCarburetor Testing

The carburetor was examined and tested at the manufacturer's facility on May 26, 2015, with an FAA inspector present. Initial flow testing revealed that the main gasket and float were misaligned; likely due to the disassembly and reassembly performed on-scene. The floats appeared to be in good condition and the arms were not damaged. The floats were aligned properly, and the carburetor was flow tested a second time at four different power settings. Throughout all power setting...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA15FA170