N162WR

Substantial
Fatal

CUB CRAFTERS CC18-180S/N: CC18-0035

Accident Details

Date
Friday, June 5, 2015
NTSB Number
CEN15FA255
Location
Raton, NM
Event ID
20150605X24005
Coordinates
36.716388, -104.133331
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot's failure to maintain adequate airspeed while maneuvering at a low altitude, which resulted in the airplane exceeding its critical angle of attack and experiencing an aerodynamic stall.

Aircraft Information

Registration
N162WR
Make
CUB CRAFTERS
Serial Number
CC18-0035
Year Built
2008
Model / ICAO
CC18-180

Registered Owner (Historical)

Name
USDA-APHIS-WS
Address
1223 N AIRPORT ROAD
Status
Deregistered
City
CEDAR CITY
State / Zip Code
UT 84721
Country
United States

Analysis

HISTORY OF FLIGHTOn June 5, 2015, about 0628 mountain daylight time, a Cub Crafters CC18-180 airplane, N162WR, was substantially damaged when it impacted terrain near Raton, New Mexico. The commercial pilot and the gunner were fatally injured. The airplane was registered to and operated by the United States Department of Agriculture (USDA) as a public aircraft. Day visual meteorological conditions prevailed for the local flight, which departed Raton Municipal Airport (RTN), Raton, New Mexico, about 0615.

The purpose of the flight was to locate and terminate coyotes in a predetermined geographic area with a history of livestock damage. A typical mission profile consisted of locating coyotes with the aid of a ground-based spotter, after which the pilot would fly a low-altitude pass and the rear-seated gunner would shoot the coyote with a shotgun. According to the ground-based spotter, on the day of the accident, the pilot established radio contact with him after the airplane had passed over the mesa that bordered the western edge of the target area. The pilot transmitted that he saw a coyote behind the spotter's position and that they were going to perform a low-altitude pass for the gunner to kill the coyote. The spotter turned around and located the coyote using his binoculars. He reported that he heard 2 to 3 shotgun blasts as the airplane passed through his field of view on a northeast heading. He remained focused on the coyote as the airplane exited his field of view; shortly thereafter, he heard it impact the ground. He looked up from his binoculars and saw that the airplane had crashed about 3/4 mile from his position. PERSONNEL INFORMATIONAccording to Federal Aviation Administration (FAA) records, the 54-year-old pilot held a commercial pilot certificate with single-engine land and instrument airplane ratings. The pilot's last aviation medical examination was completed on June 11, 2014, when he was issued a second-class medical certificate with a limitation for corrective lenses. His last flight proficiency review was completed on November 20, 2014.

The pilot's flight history was established using his logbook and a field diary in which he recorded his recent flights. The final logbook entry was dated April 23, 2015, at which time he had accumulated 13,411.3 hours total flight time. According to the field diary, the pilot had accumulated 72.9 hours since the final logbook entry. At the time of the accident, the pilot had a total flight experience of 13,484.2 hours of which 13,033.6 hours were as pilot-in-command. The operator reported that nearly all of the pilot's total flight experience was flown in Piper PA-18 or Cub Crafters CC18-180 airplanes. He had flown 397.9 hours during the year before the accident, 319.5 hours during the 6 months before the accident, 142.4 hours during the 90 days before the accident, and 62.4 hours during the month before the accident. Including the accident flight, the pilot had flown 5.3 hours during the 24-hour period before the accident. AIRCRAFT INFORMATIONThe airplane was a two-seat, single-engine Cub Crafters CC18-180, serial number CC18-0035. The airplane was a high-wing monoplane with a steel tube fuselage structure and fabric covering for the wings, fuselage, and tail surfaces. The airplane was powered by a 180-horsepower, 4-cylinder Lycoming O-360-C4P engine, serial number L-42046-36E. The engine provided thrust through a fixed-pitch, two-blade, McCauley 1A200/FA8241 propeller, serial number AHA46002. The tandem seat airplane was equipped with a fixed conventional landing gear and wing flaps. The airplane had a maximum allowable takeoff weight of 2,300 pounds. The Federal Aviation Administration (FAA) issued the airplane a standard airworthiness certificate on December 29, 2008.

The airplane's recording tachometer indicated 3,125.7 hours at the accident site. The airframe had accumulated 3,125.7 hours since new. The factory-new engine was installed on February 1, 2013, at 1,992.8 tachometer hours. The engine subsequently accumulated 1,132.9 hours total time. The factory-new propeller was installed on February 4, 2013, at 1,996.9 tachometer hours. The propeller subsequently accumulated 1,128.8 hours total time. The last 100 hour/annual inspection of the airplane was completed on May 19, 2015, at 3,092.5 total airframe hours. The airplane had accumulated 33.2 hours since the inspection. A postaccident review of the maintenance records found no history of unresolved airworthiness issues.

The airplane had a total fuel capacity of 50 gallons (44 gallons usable) distributed between two wing fuel tanks. Based on available fueling records, the airplane likely departed with a full fuel load after being refueled the day before the accident with 33 gallons of 100 low-lead aviation fuel. METEOROLOGICAL INFORMATIONThe nearest aviation weather reporting station was located at Raton Municipal Airport (RTN), Raton, New Mexico, about 21 miles west of the accident site. At 0653, the RTN automated surface observing system reported: wind 050° at 7 knots, a clear sky, 10 miles surface visibility; temperature 12°C; dew point 7°C; and an altimeter setting of 30.19 inches of mercury.

The ground-based spotter reported that, at the time of the accident, the surface wind was calm to 1 mph with high altitude clouds observed to the east of the accident site. AIRPORT INFORMATIONThe airplane was a two-seat, single-engine Cub Crafters CC18-180, serial number CC18-0035. The airplane was a high-wing monoplane with a steel tube fuselage structure and fabric covering for the wings, fuselage, and tail surfaces. The airplane was powered by a 180-horsepower, 4-cylinder Lycoming O-360-C4P engine, serial number L-42046-36E. The engine provided thrust through a fixed-pitch, two-blade, McCauley 1A200/FA8241 propeller, serial number AHA46002. The tandem seat airplane was equipped with a fixed conventional landing gear and wing flaps. The airplane had a maximum allowable takeoff weight of 2,300 pounds. The Federal Aviation Administration (FAA) issued the airplane a standard airworthiness certificate on December 29, 2008.

The airplane's recording tachometer indicated 3,125.7 hours at the accident site. The airframe had accumulated 3,125.7 hours since new. The factory-new engine was installed on February 1, 2013, at 1,992.8 tachometer hours. The engine subsequently accumulated 1,132.9 hours total time. The factory-new propeller was installed on February 4, 2013, at 1,996.9 tachometer hours. The propeller subsequently accumulated 1,128.8 hours total time. The last 100 hour/annual inspection of the airplane was completed on May 19, 2015, at 3,092.5 total airframe hours. The airplane had accumulated 33.2 hours since the inspection. A postaccident review of the maintenance records found no history of unresolved airworthiness issues.

The airplane had a total fuel capacity of 50 gallons (44 gallons usable) distributed between two wing fuel tanks. Based on available fueling records, the airplane likely departed with a full fuel load after being refueled the day before the accident with 33 gallons of 100 low-lead aviation fuel. WRECKAGE AND IMPACT INFORMATIONThe airplane wreckage was located in an open pasture with no trees or other obstructions in the general vicinity of the accident site. The elevation of the accident site was 6,982 ft mean sea level (msl). The aircraft wreckage was orientated on a 010° magnetic heading. The airplane was found in a near-vertical attitude with the engine pushed back into the cabin. There was no appreciable wreckage propagation from the point-of-impact. The main wreckage consisted of the entire airframe, including all structural components and flight control surfaces. Flight control cable continuity was established from the forward cockpit controls to the individual control surfaces. The rear-seat control stick had been removed for the accident flight. The elevator trim jack screw was found in a neutral position. The cockpit flap handle was displaced aft during impact; however, the wing flaps appeared to be in the fully retracted position. Both wing tanks were damaged during the accident and did not contain any residual fuel; however, first responders reported that there was a substantial fuel odor at the accident site. The cockpit fuel selector was found in the BOTH position. The fuel filter assembly contained a fluid consistent in color and odor to 100 low-lead aviation fuel. The fuel filter assembly fuel sample did not exhibit water or particulate contamination. The magneto switch was observed in the BOTH position before it was turned OFF by first responders. The stall warning horn was extracted from the right wing root and rewired to the wing-mounted lift sensor switch. Although the lift sensor switch had evidence of impact damage, the stall warning horn produced an aural tone when electrical power was applied and the switch contact was closed. The airspeed indicator exhibited a visible outline of the pointer that had been deposited on the gauge face. The observed white outline was pointed toward 69 mph. The propeller had separated from the engine crankshaft flange and was buried about 4 inches into the ground. The propeller blades exhibited S-shape spanwise bending, chordwise scratches and burnishing, and a leading-edge gouge.

The engine remained partially attached to the firewall by its mounts and control cables. Mechanical continuity was confirmed from the engine components to their respective cockpit controls. Internal engine and valve train continuity was confirmed as the engine crankshaft was rotated. Compression and suction were noted on all cylinders in conjunction with crankshaft rotation. The upper spark plugs were removed and exhibited features consistent with normal engine operation. Both magnetos provided spark on all leads when rotated. There were no obstructions between the air filter housing and the carburetor. The carburetor fuel bowl contained a liquid tha...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN15FA255