N8598H

Substantial
Minor

GRUMMAN ACFT ENG COR-SCHWEIZER G 164AS/N: 1429

Accident Details

Date
Sunday, June 21, 2015
NTSB Number
WPR15LA194
Location
Five Points, CA
Event ID
20150622X43026
Coordinates
36.429721, -120.103057
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

Maintenance personnel’s improper reassembly of the engine during overhaul, which led to the failure of the supercharger-blower due to a lack of lubrication and the subsequent total loss of engine power during takeoff.

Aircraft Information

Registration
N8598H
Make
GRUMMAN ACFT ENG COR-SCHWEIZER
Serial Number
1429
Engine Type
Turbo-shaft
Year Built
1975
Model / ICAO
G 164AG64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
8562 AGUAS FRIAS RD
Status
Deregistered
City
CHICO
State / Zip Code
CA 95928-9521
Country
United States

Analysis

On June 21, 2015, about 0600 Pacific daylight time, a Grumman Aircraft ENG COR-Schweizer G 164A, N8598H, sustained substantial damage following a loss of engine power and subsequent emergency landing near Fresno, California. The airplane was registered to, and operated by, Kenny's Crop Dusting, Inc., under the provisions of 14 Code of Federal Regulations (CFR) Part 137 as an aerial application flight. The pilot, the sole occupant, was not injured. Visual meteorological conditions prevailed for the flight, which operated without a flight plan. The local flight was departing a private airstrip at the time of the accident.

The pilot reported that shortly after takeoff, about 50 feet above ground level, the engine lost power. The pilot initiated a forced landing to a field. The airplane impacted the ground and came to rest inverted.

On August 5, 2015, the engine was examined at the facilities of Tulsa Aircraft Engines, Tulsa, Oklahoma. A complete report on the examination is part of the public docket for this accident. The starter drive gear was locked, and unable to rotate by hand inside the blower assembly. The starter drive gear exhibited heat bluing. The starter shaft circumference measured the same dimensions as the starter shaft bushing; there was zero (0) side clearance/tolerance. To lubricate the shaft and the bearings, oil was directed from a hole inside the starter shaft bushing. The Pratt & Whitney R-1340 engine table of limits indicated that the minimum required side clearance/tolerance between the starter shaft and the starter shaft bushing was 0.002 inches.

The examination revealed that the engine's blower had failed due to lack of lubrication to the impeller shaft and bearings.

At the time of the accident, the engine had accumulated 2.0 hours since its last major overhaul. A review of maintenance records showed that the last major overhaul was dated February 21, 2013, at a total aircraft time of 3,952.76 hours. The engine was installed on the airplane on June 4, 2015.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR15LA194