Accident Details
Probable Cause and Findings
The pilot's failure to maintain clearance from terrain during low-level airwork, which resulted in uncontrolled collision with terrain. Contributing to the accident was the pilot's impairment from the combined effects of butalbital and codeine.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHTOn June 22, 2015, about 0930 Pacific daylight time, an experimental, exhibition-category Short Brothers PLC S312 Tucano T MK 1 airplane, N206PZ, impacted terrain about 16 miles south of Maricopa, California. The private pilot was fatally injured, and the airplane was destroyed. The airplane was registered to Tucano Flyer LLC and was being operated as a 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions existed near the accident site about the time of the accident, and a flight plan had not been filed. The flight originated from Camarillo Airport (CMA), Camarillo, California, at 0810.
According to the air traffic control (ATC) communications, the pilot was in contact with the Southern California Air Route Traffic Control Center and was receiving advisories while performing airwork. At 0823, the pilot informed the controller that he would be performing airwork between 2,500 and 10,000 ft mean sea level (msl). The controller explained that he would probably lose radio contact and would not be able to provide flight following below 7,000 ft msl. The pilot replied that he understood and would be performing airwork for about 1 hour before returning to CMA. The controller continued to monitor the airplane during the flight. At 0924, the pilot advised the controller that he would be descending and that he may lose him for a few minutes. He added that he would then climb to 9,000 ft msl and return to CMA, and the controller acknowledged. Subsequently, the controller made several attempts to contact the pilot, but no further response was received from him.
Review of radar data provided by the Federal Aviation Administration (FAA) revealed a primary target, consistent with the accident airplane, performing multiple turns and rapidly changing altitude and airspeed. At 0845, the airplane was traveling on an eastbound heading at 3,400 ft above ground level (agl), and during the next 2 minutes, it climbed over rising terrain. Over the next 8 minutes, the airplane's speed varied and reached 325 knots and continued to make multiple turns and rapid changes in altitude and descended to within less than 100 ft above a mountain ridgeline. The airplane then continued to the northwest over lower terrain before turning southbound. During the next 18 minutes, the airplane performed multiple turns at altitudes between 2,000 and 3,000 ft agl. During the last 6 minutes of the flight, the airplane performed a 360° descending right turn near a residence at the lower entrance of Quatal Canyon at an altitude of about 3,600 ft, descending to 1,600 ft agl. The airplane headed westbound for 3 minutes and then returned to the lower entrance of Quatal Canyon. At 0924, the last radar targets showed the airplane heading eastbound above the canyon's dry river bed about 1,600 ft agl.
At 0925 radar contact was lost. Shortly after, an airplane in the area of the accident site reported to ATC that a small fire was located in a river bed. Local authorities responded to the fire and confirmed that it was the accident site.
A witness, located about 1 1/2 miles west of the accident site, reported seeing the airplane circle near her house about 500 to 800 ft agl. She stated that the engine sound was "loud and consistent." She added that she last saw the airplane fly eastbound, parallel to Quatal Canyon Road, and that shortly after saw dust and smoke rise high above a nearby mountain.
Another witness, located about 2 3/4 miles west-southwest of the accident site, reported seeing the airplane fly directly over his house in straight-and-level flight between 500 and 750 ft agl. He added that the engine sounded different than other airplanes that fly in the area but that it did not sound like anything was wrong. The airplane continued to fly straight and level in an easterly direction toward Quatal Canyon Road. PERSONNEL INFORMATIONThe pilot held a private pilot certificate with airplane single-engine land and rotorcraft ratings. He held an FAA second-class airman medical certificate, issued on June 19, 2015, with the limitation that he must wear corrective lenses.
According to the pilot's logbooks, he had accumulated 891.2 total flight hours in fixed wing aircraft and rotorcraft. He had accumulated 76.9 hours in the accident airplane make and model, 27.8 hours of which were in the previous 6 months. The pilot successfully completed his most recent flight review on January 14, 2015, in the accident airplane. AIRCRAFT INFORMATIONThe two-seat, low-wing airplane, serial number (S/N) T31, was manufactured in 1989. It was powered by a Honeywell (Garrett) TPE331-12B-703A engine, S/N P-65617, rated at 1,100 shaft horsepower at a propeller speed of 2,000 rpm. The airplane was equipped with a Hartzell propeller, model HC-D4N-5C. Review of the maintenance records showed that an annual inspection was completed on October 20, 2014. The airplane was produced to meet stringent military requirements and was designed for high-g landing loads; advanced fatigue testing; and spin tests, including inverted spins, at all altitude. METEOROLOGICAL INFORMATIONData recorded by the Meadows Field Airport, Bakersfield, California, automated weather observation station, located about 41 miles northeast of the accident site, included winds from 180° at 4 knots, visibility clear, temperature 24°C, dew point 3°C, and an altimeter setting of 30.01 inches of mercury. AIRPORT INFORMATIONThe two-seat, low-wing airplane, serial number (S/N) T31, was manufactured in 1989. It was powered by a Honeywell (Garrett) TPE331-12B-703A engine, S/N P-65617, rated at 1,100 shaft horsepower at a propeller speed of 2,000 rpm. The airplane was equipped with a Hartzell propeller, model HC-D4N-5C. Review of the maintenance records showed that an annual inspection was completed on October 20, 2014. The airplane was produced to meet stringent military requirements and was designed for high-g landing loads; advanced fatigue testing; and spin tests, including inverted spins, at all altitude. WRECKAGE AND IMPACT INFORMATIONExamination of the accident site revealed that the airplane was destroyed by high-impact forces and postimpact fire, which was observed along the debris path; the fire burned about 1 acre of land surrounding the accident site. The wreckage, including all major structural airplane components and primary flight controls, was located in a dry creek bed and was contained within a debris path that was about 641 ft long and 355 ft wide.
The first identified point of contact (FIPC) was a trough of disturbed ground about 2 ft wide, 20 ft long, and 1 ft deep, consistent with an airplane attitude of 45-degrees nose down and right wing downward about 90-degrees from level flight. The wreckage debris path was oriented along a magnetic heading of about 360° from the FIPC to the main wreckage. A green light emitting diode navigation light was found near the FIPC. At the end of the trough was a crater, about 11 ft in diameter and 5 ft deep. Two separated propeller blades, a landing gear strut with the wheel attached, and distorted pieces of sheet metal were found in and near the crater. The dirt in the crater was discolored and smelled of fuel. A third propeller blade, the wing and fuselage sections, and the engine bull gear assembly were found between the crater and the main wreckage.
The main wreckage was located about 180 ft from the FIPC and included the empennage, aft fuselage, firewall, and engine, and the wreckage was twisted and distorted. Wire bundles and cabin instrumentation were found with the main wreckage, and all of it was burned and crushed. The fourth propeller blade was located about 80 ft past the main wreckage. All four propeller blades revealed S-type bending, chordwise scoring, and leading-edge gouging near the tips.
The attached parachute and canopy were found in several sections past the main wreckage and in line with the center of the debris field. A single-point refueling port was found 641 ft from the FIPC and was the last piece of wreckage found along the debris path.
The aft fuselage and tail section structure were partially intact, and cable control continuity was confirmed to the midsection of the fuselage. The aileron control cables were found with the main wreckage. All primary flight controls were found in the debris field.
The engine exhibited thermal discoloration and impact damage. The first stage of the compressor section was visible, and all of the blades exhibited rotational signatures. The third stage was also visible from the damaged housing and exhibited rotational signatures.
Follow-up Examination
The wreckage was relocated to a secure facility where a layout examination took place. The examination of the wreckage revealed no evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation. The wing sections exhibited leading edge crush damage. The main spar was found in several sections with bending near the midsection. Each of the ailerons were found in two 3-ft sections. The wing flaps exhibited signatures suggesting that they were in the retracted position during impact. Both elevators and horizontal stabilizers were impact damaged and crushed. The trim actuator shaft had separated midspan, and 45° shear lips were observed on the separation surfaces. The trim actuator shaft was measured from the shaft bolt to the rubber seal and was 3.845 inches long, which equated to about a 0.5° (near neutral) pitch trim position. The rudder and vertical stabilizer sustained impact damage and remained attached via the rudder control cables. The vertical stabilizer and aft fuselage remained secure at all the attachment points.
The propeller assembly, which had separated from the engine during the accident sequence, was impact damaged. The cylinder, piston, feathering spring, and hub were found separated into numerous sections. Hub sections were removed from two of the four bla...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR15FA195