N1168Z

Substantial
None

MOONEY M20KS/N: 25-0697

Accident Details

Date
Sunday, June 21, 2015
NTSB Number
CEN15LA279
Location
Sheboygan, WI
Event ID
20150622X70018
Coordinates
43.769721, -87.851669
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Oil starvation due to preignition in the No. 5 cylinder as a result of failed spark plugs; the top and sides of the piston head were eroded, which allowed the exhaust gases caused by the preignition to pressurize the crankcase and force engine oil out of the breather tube.

Aircraft Information

Registration
N1168Z
Make
MOONEY
Serial Number
25-0697
Engine Type
Reciprocating
Year Built
1982
Model / ICAO
M20KM20T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
PAWLAK JAMES R
Address
13018 CENTERVILLE RD
Status
Deregistered
City
CLEVELAND
State / Zip Code
WI 53015-1306
Country
United States

Analysis

On June 21, 2015, about 1130 central daylight time, the pilot of a Mooney M20K, N1168Z, made a forced landing in a wheat field 5 miles south of Sheboygan (KSBM), Wisconsin. The pilot, the sole occupant on board, was not injured. The airplane was substantially damaged. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight. Instrument meteorological conditions prevailed, and an instrument flight rules flight plan had been filed and activated. The flight originated from KSBM at 1113 and was destined for Elkhart (KEKM), Indiana.Shortly after airplane departed, the pilot advised he was returning to KSBM due to low oil pressure. The airplane lost engine power and the pilot made a forced landing in a wheat field five miles south of the airport. A Federal Aviation Administration (FAA) airworthiness inspector who examined the airplane reported finding no oil in the crankcase. He reported the rear bulkhead was wrinkled and the empennage was twisted.

On July 1, 2015, an FAA airworthiness inspector examined the engine and turbocharger. He reported the turbocharger was dry and did not appear to be at fault. On August 17, the FAA airworthiness inspector examined the engine again at a teardown facility in Poplar Grove, Wisconsin. He reported finding evidence of pre-ignition in the number 5 cylinder that appeared to have been caused by failed spark plugs. The top and sides of the piston head were eroded, allowing exhaust gases to pressurize the crankcase and force engine oil out of the breather tube.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN15LA279