Accident Details
Probable Cause and Findings
A partial loss of engine power due to oil starvation. Contributing was the flight instructor's failure to maintain control of the airplane during an aborted emergency landing, and his delayed decision to deploy the airplane's parachute system.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHTOn July 22, 2015, about 1044 eastern daylight time, a Cirrus SR20, N610DA, was destroyed when it impacted terrain during a go-around at Lake Wales Municipal Airport (X07), Lake Wales, Florida. The flight instructor was seriously injured, and the private pilot receiving instruction was fatally injured. Visual meteorological conditions prevailed, and an instrument flight rules (IFR) flight plan was filed for the flight from the Orlando Sanford International Airport (SFB), Sanford, Florida to Page Field Airport (FMY), Fort Myers, Florida. The airplane was operated by Aerosim Flight Academy. The instructional flight was conducted under the provisions of 14 Code of Federal Regulations Part 91.
According to the flight instructor, he and the private pilot were in cruise flight at 5,000 feet mean sea level (msl), when air traffic control (ATC) changed their next enroute waypoint due to traffic. As the flight instructor was demonstrating how to change the route in the GPS, they noticed a "puff" of black smoke appear from under the legs of the student pilot. The smoke dissipated quickly and seconds later, the oil pressure light came on with an alarm. The flight instructor took over the flight controls and declared an emergency before diverting to X07. He maintained an altitude of 4,000 feet msl until he had the airport in sight. He made one call on the airport's common traffic advisory frequency reporting "short final for runway 17."
The flight instructor said he was, "too high and going too fast to make the runway." He side-slipped the airplane, but could not get it slowed down enough for a safe landing so he decided to abort the landing and make a 360 degree turn. He advanced the throttle but the engine did not feel like it was generating any power. He saw the adjacent runway, and although a yellow "X" was on runway, he elected to land anyway. He stated the engine lost complete power and about 400 feet above ground level (agl) he told the student pilot to deploy the airplane's emergency parachute. The parachute did not arrest the descent before the airplane entered an aerodynamic stall and crashed in wooded terrain. After the crash the flight instructor telephoned 911 and requested emergency assistance.
According to witnesses at X07, they watched as the airplane approached runway 17. They said that as the airplane reached the runway threshold the pilot appeared to abort the landing before "throttling up" and continuing to fly down the runway. The airplane then made a left turn towards the departure end of runway 6. As the airplane reached the end of the runway, witnesses reported that it seemed "slow and wobbly," before it entered a descending left turn. The witnesses also stated that the airframe parachute was deployed but not fully inflate prior to impact. PERSONNEL INFORMATIONFlight Instructor
The flight instructor, age 33, held a commercial pilot certificate for airplane single engine, multi-engine land and instrument airplane. His flight instructor certificate had ratings for airplane single-engine, multi-engine, and instrument airplane. The flight instructor's most-recent first class medical certificate was issued in April 2013, was issued without any limitations. According to records provided by the operator, the flight instructor had accumulated about 1,170 total flight hours.
Private Pilot
The private pilot, age 26, held a private pilot certificate with a rating for airplane single-engine land. He was issued a combined student pilot and first class medical certificate with limitations requiring the use of corrective lenses. A review of the pilots training records reveal that the pilot took his check ride on April 5, 2015 and received his private pilot certificate on April 13, 2015. A review of his flight training log revealed he accumulated about 70 hours of total flight experience; all of his flight experience in the accident airplane make and model. AIRCRAFT INFORMATIONThe airplane was manufactured in 2007. It was powered by a Continental IO-360-ES16B engine rated at 210 horsepower, and was equipped with a Hartzell two-blade constant-speed propeller. The last 100-hour inspection of the airframe and engine occurred on July 11, 2015, at an airframe total time of 6,263.8 hours. As of that inspection the engine had accumulated 2,046 total hours of operation.
According to Continental Motors Service Information Letter SIL 98-9C, the recommended overhaul interval for the engine was 2,200 hours. METEOROLOGICAL INFORMATIONThe nearest recorded weather at Bartow Municipal Airport Bartow, Florida (BOW) located 9 nautical miles northwest from the accident site at 1047, included winds from 250 degrees at 7 knots; 10 statute miles visibility, scattered clouds at 2,000 feet, temperature 28 degrees Celsius (C), dew point temperature 24 degrees C, and an altimeter setting of 30.02 inches of mercury. AIRPORT INFORMATIONThe airplane was manufactured in 2007. It was powered by a Continental IO-360-ES16B engine rated at 210 horsepower, and was equipped with a Hartzell two-blade constant-speed propeller. The last 100-hour inspection of the airframe and engine occurred on July 11, 2015, at an airframe total time of 6,263.8 hours. As of that inspection the engine had accumulated 2,046 total hours of operation.
According to Continental Motors Service Information Letter SIL 98-9C, the recommended overhaul interval for the engine was 2,200 hours. WRECKAGE AND IMPACT INFORMATIONExamination of the wreckage was conducted at the accident site, and all major components of the airframe were accounted for at the scene. The wreckage path was oriented on a heading of about 320 degrees magnetic, and was 46 feet in length. Examination of the right wing revealed that it was splintered and the fuel tank was breached. The cockpit was broken away from the fuselage and crushed, and the fuselage displayed crush damage throughout the hull. The empennage was intact and revealed impact damage. The left wing was intact and approximately 12 gallons of fuel were drained from the main tank. Flight control continuity was established from the cockpit controls to all flight control surfaces. A cursory examination of the engine revealed that it was impact-damaged and crushed aft towards the firewall. The propeller was fractured off of the engine crankshaft and located in the debris path approximately 20 feet from the main wreckage. Further examination of the fuselage revealed that the Cirrus Airframe Parachute System (CAPS) was deployed and located 320 degrees magnetic and approximately 226 feet from the main wreckage.
Examination of the engine revealed that it was impact-damaged.. The exhaust pipes were crushed. The rocker covers and top spark plugs were removed, and the cylinders were examined using a lighted borescope. All of the pistons and cylinder domes exhibited normal combustion deposits, and the valves were in place. Further examination of the pistons revealed that the oil ports on the pistons were clogged and coking was present. The oil control rings on all pistons were "stuck." The Nos. 1, 2 and 3 connecting rod bearings showed evidence of incipient oil starvation. Examination of the crankshaft revealed it was broken at the flange where it entered the crankcase halves. The remainder of the crankshaft had continuity when it was rotated. Thumb compression was obtained on all of the cylinders. The camshaft was observed when the oil sump was removed and was coated with oil. The oil sump was removed and examined. The sump was impact damaged and the broken part of the sump that held the oil plug was not located. A small amount of oil was observed in the bottom of the remaining portion of the sump and no metal particles were observed. A large amount of oil residue noted on the belly of the airplane.
The top spark plugs were removed and examined. They exhibited normal wear and had light gray deposits in the electrode areas. The bottom spark plugs were examined with the borescope and they appeared similar to the top spark plugs. The top number one spark plug was broken. An examination of the magnetos revealed a hole was observed in the side of the left magneto. The right magneto was in place and not damaged. Both magnetos sparked at all terminals when the drive shafts were rotated.
Examination of the fuel pump revealed that it was in secure to the engine and impact damaged. The mixture control was still connected and bent to the rear. The drive coupling was not damaged. The drive shaft was free to rotate. The vapor return line was separated, along with the exit line to the metering unit. The unit was disassembled and no internal damage was observed. Examination of the throttle body and metering unit revealed that it was impact damaged.
The throttle control was free to move. The metering unit was disassembled and no internal damage was observed. The fuel nozzles were in place on the cylinders. Nozzles 2 and 5 were impact damaged. All of the nozzles were clear.
Examination of the accessory case and oil pump revealed that the oil screen was clean, free of debris and coated with oil. The oil pump was in place and the shaft was free to rotate. The pump was disassembled and the pump gears were coated with oil and were not damaged. The oil filter was separated from the engine and not located.
Examination of the propeller revealed that it had separated from the engine during the impact sequence; the engine crankshaft fractured aft of the propeller mounting flange. The propeller assembly with spinner was intact but damaged. Both blades appeared to be resting on the low pitch setting and exhibited noticeable chordwise abrasion in the tip area on the camber side. One blade exhibited an S-bending and twisted leading edge down. Impact marks on one of the blades and on its preload plates indicated the propeller was in the normal operating blade angle range prior to impact. ADDITIONAL INFORMATIONAirframe Parachute System
The airplane was equ...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA15FA277