N963X

Substantial
Minor

GRUMMAN G-164AS/N: 477

Accident Details

Date
Friday, July 31, 2015
NTSB Number
CEN15LA330
Location
Emmett, KS
Event ID
20150801X23811
Coordinates
39.307220, -96.056388
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The engine failure due to several loose, damaged cylinder stud nuts and hold-down bolts. Contributing to the accident was maintenance personnel’s failure to detect that the cylinder nuts and hold-down bolts were not properly secured during the engine’s most recent inspection.

Aircraft Information

Registration
N963X
Make
GRUMMAN
Serial Number
477
Engine Type
Turbo-shaft
Year Built
1968
Model / ICAO
G-164AG64T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
PO BOX 482
Status
Deregistered
City
WALNUT RIDGE
State / Zip Code
AR 72476-0482
Country
United States

Analysis

On June 31, 2015, about 1130 central daylight time, a Grumman G-164A, N963X, impacted terrain after the engine lost power near Emmett, Kansas. The pilot, the sole occupant on board, received minor injuries. The airplane was substantially damaged. The airplane was registered to and operated by Precision Aerial Ag LLC of Seneca, Kansas, under the provisions of 14 Code of Federal Regulations Part 137 as an aerial application flight. Visual meteorological conditions prevailed at the time of the accident, and no flight plan had been filed. The local flight originated from Wamego, Kansas approximately 1100.According to the pilot's accident report, he was making a spray run when he heard a loud "bang," saw a puff of smoke emit from the upper right-hand side of the engine, and then the propeller seized. He made a forced landing in a brome field, collided with some bushes, and nosed over. Examination of the engine on-site by inspectors from the Federal Aviation Administration revealed several loose cylinder stud nuts and hold-down bolts that appeared to have been pushed up on the cylinder skirt. Several of the studs – number 4 cylinder in particular -- were stretched and looked to be nearly pushed out of the engine crankcase. One cylinder was about to separate from crankcase.

Examination of the engine maintenance logbook revealed the engine had received a major overhaul on February 13, 2007. On March 10, 2010, Airworthiness Directive (A.D.) 99-11-02 was complied with by inspecting the cylinder heads. On March 2, 2011, February 22, 2012, May 30, 2013, and May 13, 2014, A.D. 56-06-02 was complied with by inspecting the cylinder hold-down studs. On July 15, 2014, the engine and propeller were removed due to a blower bearing failure. On August 10, 2014, after the engine and propeller were reinstalled, and again on March 18, 2015, the cylinder bases and heads were checked for cracks and loose studs. At the time of the last inspection, the tachometer read 6,730 hours, and the engine had accrued 506.68 hours since major overhaul.

The accident site was located at 14624 A4 Road, Emmett, Kansas.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN15LA330