Summary
On September 07, 2015, a Piper PA 28R-200 (N1125X) was involved in an incident near Doylestown, PA. All 1 person aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's failure to land with sufficient runway remaining to safely stop the airplane. Contributing to the accident was the pilot's fatigue during the flight.
The pilot reported that during the landing, she "landed at the last 1000' of available runway and attempted to stop the aircraft using toe brakes and aerodynamic braking, but this was insufficient." The airplane departed the runway into the grass and the right wing struck a taxiway light. A postflight inspection revealed substantial damage to the right wing.
The pilot also stated, "I feel this accident could have been prevented by executing a go-around and trying a lower approach as opposed to trying to save the landing. I attribute this lack of judgment to fatigue."
The pilot reported there were no pre-impact mechanical failures or malfunctions with the airframe or engine that would have precluded normal operation.
This incident is documented in NTSB report GAA15CA263. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N1125X.
Accident Details
Probable Cause and Findings
The pilot's failure to land with sufficient runway remaining to safely stop the airplane. Contributing to the accident was the pilot's fatigue during the flight.
Aircraft Information
Registered Owner (Current)
Analysis
The pilot reported that during the landing, she "landed at the last 1000' of available runway and attempted to stop the aircraft using toe brakes and aerodynamic braking, but this was insufficient." The airplane departed the runway into the grass and the right wing struck a taxiway light. A postflight inspection revealed substantial damage to the right wing.
The pilot also stated, "I feel this accident could have been prevented by executing a go-around and trying a lower approach as opposed to trying to save the landing. I attribute this lack of judgment to fatigue."
The pilot reported there were no pre-impact mechanical failures or malfunctions with the airframe or engine that would have precluded normal operation.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# GAA15CA263